Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Texas A&M, College Station |
---|---|
Assessment Year | 1990 |
Principal Product | MACHINE SHOP JOBS |
NAICS | n/a |
SIC | 3599 - Industrial Machinery, Nec |
Sales | $10,000,000-$50,000,000 |
# of Employees | 70 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 642 Pieces |
Production Hrs. Annual | 4,832 |
Location (State) | TX |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $223,672 | 3,633,060 | kWh | $0.06 |
Natural Gas | $44,235 | 8,690 | MMBtu | $5.09 |
TOTAL ENERGY COSTS | $267,907 | |||
RECOMMENDED SAVINGS* | $54,756 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $54,756 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4324 REPLACE HYDRAULIC / PNEUMATIC EQUIPMENT WITH ELECTRIC EQUIPMENT |
Savings: $31,894 Cost: $22,000 |
$31,894 | 732,708 | - | - |
$31,894 732,708 kWh |
- - MMBtu |
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02: 2.6232 INSTALL SET-BACK TIMERS |
Savings: $8,700 Cost: $450 |
$8,700 | 195,487 | - | - |
$8,700 195,487 kWh |
- - MMBtu |
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03: 2.7121 UTILIZE DAYLIGHT WHENEVER POSSIBLE IN LIEU OF ARTIFICIAL LIGHT |
Savings: $6,807 Cost: $7,920 |
$6,807 | 152,989 | - | - |
$6,807 152,989 kWh |
- - MMBtu |
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04: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $2,870 Cost: $3,160 |
- | - | $2,870 | 560 |
- - kWh |
$2,870 560 MMBtu |
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05: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $2,260 Cost: $675 |
$2,260 | 38,394 | - | - |
$2,260 38,394 kWh |
- - MMBtu |
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06: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $670 Cost: - |
$670 | 15,240 | - | - |
$670 15,240 kWh |
- - MMBtu |
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07: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $715 Cost: $500 |
$715 | 16,120 | - | - |
$715 16,120 kWh |
- - MMBtu |
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08: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $580 Cost: $270 |
- | - | $580 | 113 |
- - kWh |
$580 113 MMBtu |
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09: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $260 Cost: - |
$260 | 5,862 | - | - |
$260 5,862 kWh |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $54,756 Cost: $34,975 |
$51,306 | 1,156,800 | $3,450 | 673 | $51,306 1,156,800 kWh |
$3,450 673 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $54,756 Cost: $34,975 |
$51,306 | 1,156,800 | $3,450 | 673 | $51,306 1,156,800 kWh |
$3,450 673 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |