Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Texas A&M, College Station |
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Assessment Year | 2003 |
Principal Product | Lime processing |
NAICS | 327410 - Lime Manufacturing |
SIC | 3274 - Lime |
Sales | $10,000,000-$50,000,000 |
# of Employees | 70 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 400,000 Tons |
Production Hrs. Annual | 8,400 |
Location (State) | TX |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $1,053,076 | 24,791,400 | kWh | $0.04 |
Electricity Demand | $15,942 | 29,952 | kW-months/year | $0.53 |
Natural Gas | $4,063,260 | 1,054,610 | MMBtu | $3.85 |
TOTAL ENERGY COSTS | $5,132,278 | |||
RECOMMENDED SAVINGS* | $19,800 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $15,620 |
#|Description |
Savings Cost |
Status | Electricity Usage | Personnel Changes | Electricity Usage | Personnel Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 4.652 REPLACE EXISTING EQUIPMENT WITH MORE SUITABLE SUBSTITUTES |
Savings: $13,600 Cost: $4,000 |
- | - | $13,600 | - |
- - kWh |
$13,600 - $ |
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02: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $4,180 Cost: $500 |
$4,180 | 110,000 | - | - |
$4,180 110,000 kWh |
- - $ |
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03: 2.7124 MAKE A PRACTICE OF TURNING OFF LIGHTS WHEN NOT NEEDED |
Savings: $2,020 Cost: - |
$2,020 | 53,270 | - | - |
$2,020 53,270 kWh |
- - $ |
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TOTAL RECOMMENDED |
Savings: $19,800 Cost: $4,500 |
$6,200 | 163,270 | $13,600 | - | $6,200 163,270 kWh |
$13,600 - $ |
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TOTAL IMPLEMENTED |
Savings: $15,620 Cost: $4,000 |
$2,020 | 53,270 | $13,600 | - | $2,020 53,270 kWh |
$13,600 - $ |
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Savings Cost |
$ | kWh | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Personnel Changes | Electricity Usage | Personnel Changes |