Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | North Carolina A&T |
---|---|
Assessment Year | 1989 |
Principal Product | HOSIERY & SOCKS |
NAICS | n/a |
SIC | 2252 - Hosiery, Nec |
Sales | $10,000,000-$50,000,000 |
# of Employees | 175 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 120,000 Pieces |
Production Hrs. Annual | 6,000 |
Location (State) | NC |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $193,553 | 3,475,381 | kWh | $0.06 |
Natural Gas | $12,600 | 3,219 | MMBtu | $3.91 |
Fuel Oil #2 | $41,553 | 11,875 | MMBtu | $3.50 |
TOTAL ENERGY COSTS | $247,706 | |||
RECOMMENDED SAVINGS* | $22,114 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $12,480 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Fuel Oil #2 | Administrative Changes | Electricity Usage | Natural Gas | Fuel Oil #2 | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.6232 INSTALL SET-BACK TIMERS |
Savings: $2,653 Cost: $2,068 |
$2,653 | 47,773 | - | - | - | - | - | - |
$2,653 47,773 kWh |
- - MMBtu |
- - MMBtu |
- - $ |
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02: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $3,019 Cost: - |
$3,019 | 54,220 | - | - | - | - | - | - |
$3,019 54,220 kWh |
- - MMBtu |
- - MMBtu |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $821 Cost: - |
$821 | 14,654 | - | - | - | - | - | - |
$821 14,654 kWh |
- - MMBtu |
- - MMBtu |
- - $ |
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04: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $1,359 Cost: $100 |
$1,359 | 24,326 | - | - | - | - | - | - |
$1,359 24,326 kWh |
- - MMBtu |
- - MMBtu |
- - $ |
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05: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS |
Savings: $127 Cost: $300 |
$127 | 2,345 | - | - | - | - | - | - |
$127 2,345 kWh |
- - MMBtu |
- - MMBtu |
- - $ |
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06: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS |
Savings: $605 Cost: $600 |
$605 | 10,844 | - | - | - | - | - | - |
$605 10,844 kWh |
- - MMBtu |
- - MMBtu |
- - $ |
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07: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $5,794 Cost: $10,000 |
- | - | $1,345 | 344 | $4,449 | 1,271 | - | - |
- - kWh |
$1,345 344 MMBtu |
$4,449 1,271 MMBtu |
- - $ |
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08: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $5,036 Cost: $50 |
- | - | $1,169 | 299 | $3,867 | 1,105 | - | - |
- - kWh |
$1,169 299 MMBtu |
$3,867 1,105 MMBtu |
- - $ |
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09: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $2,700 Cost: - |
- | - | $673 | 172 | $2,227 | 636 | $(-200) | - |
- - kWh |
$673 172 MMBtu |
$2,227 636 MMBtu |
$(-200) - $ |
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TOTAL RECOMMENDED |
Savings: $22,114 Cost: $13,118 |
$8,584 | 154,162 | $3,187 | 815 | $10,543 | 3,012 | $(-200) | - | $8,584 154,162 kWh |
$3,187 815 MMBtu |
$10,543 3,012 MMBtu |
$(-200) - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $12,480 Cost: $3,118 |
$4,744 | 85,288 | $1,842 | 471 | $6,094 | 1,741 | $(-200) | - | $4,744 85,288 kWh |
$1,842 471 MMBtu |
$6,094 1,741 MMBtu |
$(-200) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Fuel Oil #2 | Administrative Changes | Electricity Usage | Natural Gas | Fuel Oil #2 | Administrative Changes |