Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Boise State University |
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Assessment Year | 2014 |
Principal Product | Aerospace friction/brake materials |
NAICS | 336413 - Other Aircraft Parts and Auxiliary Equipment Manufacturing |
SIC | 3728 - Aircraft Parts And Equipment, Nec |
Sales | $10,000,000-$50,000,000 |
# of Employees | 156 |
Plant Area (Sq.Ft.) | 140,000 |
Annual Production | 640,000 Pounds |
Production Hrs. Annual | 8,736 |
Location (State) | WA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $2,888,403 | 56,001,943 | kWh | $0.05 |
Electricity Demand | $542,289 | 108,495 | kW-months/year | $5.00 |
Natural Gas | $374,236 | 573,778 | MMBtu | $0.65 |
TOTAL ENERGY COSTS | $3,804,927 | |||
RECOMMENDED SAVINGS* | $14,842 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $7,042 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $7,042 Cost: $1,697 |
$7,042 | 135,424 | - | - |
$7,042 135,424 kWh |
- - MMBtu |
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02: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES |
Savings: $4,268 Cost: $11,600 |
$4,268 | 82,083 | - | - |
$4,268 82,083 kWh |
- - MMBtu |
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03: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $1,073 Cost: $23,840 |
$1,073 | 20,643 | - | - |
$1,073 20,643 kWh |
- - MMBtu |
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04: 2.2424 USE HEAT IN FLUE GASES TO PREHEAT PRODUCTS OR MATERIALS |
Savings: $2,459 Cost: $2,500 |
- | - | $2,459 | 3,783 |
- - kWh |
$2,459 3,783 MMBtu |
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TOTAL RECOMMENDED |
Savings: $14,842 Cost: $39,637 |
$12,383 | 238,150 | $2,459 | 3,783 | $12,383 238,150 kWh |
$2,459 3,783 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $7,042 Cost: $1,697 |
$7,042 | 135,424 | - | - | $7,042 135,424 kWh |
- - MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |