Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of North Carolina, Charlotte |
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Assessment Year | 2023 |
Principal Product | Plywood Frames |
NAICS | 337122 - Nonupholstered Wood Household Furniture Manufacturing |
SIC | 2511 - Wood Household Furniture |
Sales | $10,000,000-$50,000,000 |
# of Employees | 100 |
Plant Area (Sq.Ft.) | 84,500 |
Annual Production | 80,000 Pieces |
Production Hrs. Annual | 5,460 |
Location (State) | NC |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $190,492 | 3,473,198 | kWh | $0.05 |
Electricity Demand | $105,172 | 8,827 | kW-months/year | $11.91 |
Electricity Fees | $2,323 | - | $ | - |
LPG | $29,396 | 1,352 | MMBtu | $21.75 |
TOTAL ENERGY COSTS | $327,383 | |||
RECOMMENDED SAVINGS* | $71,418 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Electricity Demand | LPG | Electricity Usage | Electricity Demand | LPG | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | kW-months/year | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT |
Savings: $12,780 Cost: $15,000 |
- | - | - | - | $12,780 | 588 |
- - kWh |
- - kW-months/year |
$12,780 588 MMBtu |
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02: 2.6231 UTILIZE CONTROLS TO OPERATE EQUIPMENT ONLY WHEN NEEDED |
Savings: $14,525 Cost: $19,500 |
$14,525 | 264,092 | - | - | - | - |
$14,525 264,092 kWh |
- - kW-months/year |
- - MMBtu |
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03: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES |
Savings: $34,115 Cost: $205,795 |
$23,320 | 424,008 | $10,795 | 906 | - | - |
$23,320 424,008 kWh |
$10,795 906 kW-months/year |
- - MMBtu |
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04: 2.6231 UTILIZE CONTROLS TO OPERATE EQUIPMENT ONLY WHEN NEEDED |
Savings: $147 Cost: $340 |
$147 | 2,680 | - | - | - | - |
$147 2,680 kWh |
- - kW-months/year |
- - MMBtu |
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05: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $3,751 Cost: - |
$2,564 | 46,613 | $1,187 | 100 | - | - |
$2,564 46,613 kWh |
$1,187 100 kW-months/year |
- - MMBtu |
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06: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $6,100 Cost: $3,000 |
$4,170 | 75,816 | $1,930 | 162 | - | - |
$4,170 75,816 kWh |
$1,930 162 kW-months/year |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $71,418 Cost: $243,635 |
$44,726 | 813,209 | $13,912 | 1,168 | $12,780 | 588 | $44,726 813,209 kWh |
$13,912 1,168 kW-months/year |
$12,780 588 MMBtu |
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TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - | - | - - kWh |
- - kW-months/year |
- - MMBtu |
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Savings Cost |
$ | kWh | $ | kW-months/year | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Electricity Demand | LPG | Electricity Usage | Electricity Demand | LPG |