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IAC Assessment: GT0699
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IAC Assessment: GT0699
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IAC Center Georgia Institute of Technology
Assessment Year 2000
Principal Product Poultry
NAICS n/a
SIC 2015 - Poultry Slaughtering And Processing
Sales $50,000,000-$100,000,000
# of Employees 420
Plant Area (Sq.Ft.) 250,000
Annual Production 27,000,000 Pieces
Production Hrs. Annual 2,000
Location (State) GA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $587,649 9,033,119 kWh $0.07
Electricity Demand $105,464 19,337 kW-months/year $5.45
Electricity Fees $86,083 - $ -
LPG $825,000 138,000 MMBtu $5.98
TOTAL ENERGY COSTS $1,604,196
RECOMMENDED SAVINGS* $352,413 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Electricity Demand Electricity Fees LPG Personnel Changes Electricity Usage Electricity Demand Electricity Fees LPG Personnel Changes
$ kWh $ kW-months/year $ $ $ MMBtu $ $
01: 4.4520 ELIMINATE SHIFT Savings:
$244,498
Cost:
-
$448 9,672 - - - - $28,050 4,690 $216,000 - $448
9,672
kWh
-
-
kW-months/year
-
-
$
$28,050
4,690
MMBtu
$216,000
-
$
02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$20,694
Cost:
-
$15,235 347,304 $4,284 785 $1,175 - - - - - $15,235
347,304
kWh
$4,284
785
kW-months/year
$1,175
-
$
-
-
MMBtu
-
-
$
03: 2.2522 ISOLATE HOT OR COLD EQUIPMENT Savings:
$37,855
Cost:
-
- - - - - - $37,855 6,332 - - -
-
kWh
-
-
kW-months/year
-
-
$
$37,855
6,332
MMBtu
-
-
$
04: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$8,198
Cost:
$1,000
- - - - - - $8,198 1,455 - - -
-
kWh
-
-
kW-months/year
-
-
$
$8,198
1,455
MMBtu
-
-
$
05: 2.2511 INSULATE BARE EQUIPMENT Savings:
$5,763
Cost:
$3,000
- - - - - - $5,763 949 - - -
-
kWh
-
-
kW-months/year
-
-
$
$5,763
949
MMBtu
-
-
$
06: 3.4151 MINIMIZE WATER USAGE Savings:
$680
Cost:
$600
$680 14,654 - - - - - - - - $680
14,654
kWh
-
-
kW-months/year
-
-
$
-
-
MMBtu
-
-
$
07: 3.4156 USE FLOW CONTROL VALVES ON EQUIPMENT TO OPTIMIZE WATER USE Savings:
$883
Cost:
$9,000
$833 19,050 - - $50 - - - - - $833
19,050
kWh
-
-
kW-months/year
$50
-
$
-
-
MMBtu
-
-
$
08: 3.4156 USE FLOW CONTROL VALVES ON EQUIPMENT TO OPTIMIZE WATER USE Savings:
$505
Cost:
$900
$476 10,844 - - $29 - - - - - $476
10,844
kWh
-
-
kW-months/year
$29
-
$
-
-
MMBtu
-
-
$
09: 2.6231 UTILIZE CONTROLS TO OPERATE EQUIPMENT ONLY WHEN NEEDED Savings:
$11,182
Cost:
$31,500
$421 9,086 - - - - $10,761 1,800 - - $421
9,086
kWh
-
-
kW-months/year
-
-
$
$10,761
1,800
MMBtu
-
-
$
10: 2.8112 COMBINE UTILITY METERS Savings:
$21,948
Cost:
-
- - - - $21,948 - - - - - -
-
kWh
-
-
kW-months/year
$21,948
-
$
-
-
MMBtu
-
-
$
11: 3.4151 MINIMIZE WATER USAGE Savings:
$207
Cost:
$205
$207 4,689 - - - - - - - - $207
4,689
kWh
-
-
kW-months/year
-
-
$
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$352,413
Cost:
$46,205
$18,300 415,299 $4,284 785 $23,202 - $90,627 15,226 $216,000 - $18,300
415,299
kWh
$4,284
785
kW-months/year
$23,202
-
$
$90,627
15,226
MMBtu
$216,000
-
$
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - - - - - -
-
kWh
-
-
kW-months/year
-
-
$
-
-
MMBtu
-
-
$
Savings
Cost
$ kWh $ kW-months/year $ $ $ MMBtu $ $
Electricity Usage Electricity Demand Electricity Fees LPG Personnel Changes Electricity Usage Electricity Demand Electricity Fees LPG Personnel Changes