Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Univ. of Kansas |
---|---|
Assessment Year | 1984 |
Principal Product | FIBERGLASS CAMPER SHELLS |
NAICS | n/a |
SIC | 3792 - Travel Trailers And Campers |
Sales | $5,000,000-$10,000,000 |
# of Employees | 75 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 10,000 Pieces |
Production Hrs. Annual | 4,800 |
Location (State) | KS |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $25,704 | 309,203 | kWh | $0.08 |
Natural Gas | $23,581 | 4,610 | MMBtu | $5.12 |
TOTAL ENERGY COSTS | $49,285 | |||
RECOMMENDED SAVINGS* | $15,271 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $11,864 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $4,484 Cost: $300 |
$4,484 | 53,927 | - | - | - | - |
$4,484 53,927 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.1123 INSTALL AUTOMATIC STACK DAMPER |
Savings: $4,147 Cost: $3,200 |
- | - | $4,147 | 810 | - | - |
- - kWh |
$4,147 810 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.2532 USE ONLY AMOUNT OF AIR NECESSARY TO PREVENT EXPLOSION HAZARD |
Savings: $2,531 Cost: $178 |
$268 | 3,224 | $2,263 | 442 | - | - |
$268 3,224 kWh |
$2,263 442 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
04: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $2,023 Cost: $1,273 |
$2,023 | 24,326 | - | - | - | - |
$2,023 24,326 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
05: 2.1232 KEEP BOILER TUBES CLEAN |
Savings: $942 Cost: $64 |
- | - | $942 | 184 | - | - |
- - kWh |
$942 184 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
06: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT |
Savings: $876 Cost: $1,200 |
- | - | $876 | 171 | - | - |
- - kWh |
$876 171 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
07: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $268 Cost: $50 |
- | - | $768 | 150 | $(-500) | - |
- - kWh |
$768 150 MMBtu |
$(-500) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $15,271 Cost: $6,265 |
$6,775 | 81,477 | $8,996 | 1,757 | $(-500) | - | $6,775 81,477 kWh |
$8,996 1,757 MMBtu |
$(-500) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $11,864 Cost: $4,887 |
$6,507 | 78,253 | $5,857 | 1,144 | $(-500) | - | $6,507 78,253 kWh |
$5,857 1,144 MMBtu |
$(-500) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |