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IAC Assessment: KU0342
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IAC Assessment: KU0342
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IAC Center Univ. of Kansas
Assessment Year 1991
Principal Product CENTRIFUGAL PUMPS
NAICS n/a
SIC 3561 - Pumps And Pumping Equipment
Sales $50,000,000-$100,000,000
# of Employees 300
Plant Area (Sq.Ft.) 0
Annual Production 0 Units
Production Hrs. Annual 4,190
Location (State) KS
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $262,587 4,654,748 kWh $0.06
Natural Gas $45,353 15,663 MMBtu $2.90
TOTAL ENERGY COSTS $307,940
RECOMMENDED SAVINGS* $37,775 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas Electricity Usage Natural Gas
$ kWh $ MMBtu
01: 2.4239 ELIMINATE OR REDUCE COMPRESSED AIR USAGE Savings:
$12,017
Cost:
$3,600
$12,017 213,072 - - $12,017
213,072
kWh
-
-
MMBtu
02: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS Savings:
$8,091
Cost:
$9,690
- - $8,091 2,790 -
-
kWh
$8,091
2,790
MMBtu
03: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS Savings:
$774
Cost:
$1,140
$264 4,689 $510 176 $264
4,689
kWh
$510
176
MMBtu
04: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$7,753
Cost:
$500
$7,753 137,456 - - $7,753
137,456
kWh
-
-
MMBtu
05: 2.3512 DE-ENERGIZE EXCESS TRANSFORMER CAPACITY Savings:
$4,942
Cost:
$100,000
$4,942 87,632 - - $4,942
87,632
kWh
-
-
MMBtu
06: 2.6232 INSTALL SET-BACK TIMERS Savings:
$2,678
Cost:
$550
$2,678 47,479 - - $2,678
47,479
kWh
-
-
MMBtu
07: 2.7314 REDUCE VENTILATION AIR Savings:
$1,195
Cost:
$200
$397 7,034 $798 275 $397
7,034
kWh
$798
275
MMBtu
08: 2.7221 LOWER TEMPERATURE DURING THE WINTER SEASON AND VICE-VERSA Savings:
$325
Cost:
-
- - $325 112 -
-
kWh
$325
112
MMBtu
TOTAL RECOMMENDED Savings:
$37,775
Cost:
$115,680
$28,051 497,362 $9,724 3,353 $28,051
497,362
kWh
$9,724
3,353
MMBtu
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - -
-
kWh
-
-
MMBtu
Savings
Cost
$ kWh $ MMBtu
Electricity Usage Natural Gas Electricity Usage Natural Gas