Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Louisiana Tech |
---|---|
Assessment Year | 1986 |
Principal Product | PRESTRESSED CONCRETE |
NAICS | n/a |
SIC | 3272 - Concrete Products, Nec |
Sales | $1,000,000-$5,000,000 |
# of Employees | 25 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 27,000 Thousand Feet |
Production Hrs. Annual | 2,210 |
Location (State) | LA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $17,226 | 138,042 | kWh | $0.12 |
Natural Gas | $72,564 | 16,933 | MMBtu | $4.29 |
TOTAL ENERGY COSTS | $89,790 | |||
RECOMMENDED SAVINGS* | $23,902 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $7,107 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $3,910 Cost: - |
$3,910 | 47,479 | - | - | - | - |
$3,910 47,479 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $575 Cost: - |
$575 | 7,034 | - | - | - | - |
$575 7,034 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.2515 USE OPTIMUM THICKNESS INSULATION |
Savings: $11,458 Cost: $28,763 |
- | - | $9,438 | 2,200 | $2,020 | - |
- - kWh |
$9,438 2,200 MMBtu |
$2,020 - $ |
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05: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $2,214 Cost: $2,000 |
- | - | $2,214 | 516 | - | - |
- - kWh |
$2,214 516 MMBtu |
- - $ |
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06: 2.1232 KEEP BOILER TUBES CLEAN |
Savings: $1,737 Cost: $3,000 |
- | - | $1,737 | 405 | - | - |
- - kWh |
$1,737 405 MMBtu |
- - $ |
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07: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $3,600 Cost: $10,000 |
- | - | $3,600 | 840 | - | - |
- - kWh |
$3,600 840 MMBtu |
- - $ |
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08: 2.1131 REPAIR FAULTY INSULATION IN FURNACES, BOILERS, ETC |
Savings: $408 Cost: $1,000 |
- | - | $408 | 95 | - | - |
- - kWh |
$408 95 MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $23,902 Cost: $44,763 |
$4,485 | 54,513 | $17,397 | 4,056 | $2,020 | - | $4,485 54,513 kWh |
$17,397 4,056 MMBtu |
$2,020 - $ |
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TOTAL IMPLEMENTED |
Savings: $7,107 Cost: $3,000 |
$4,485 | 54,513 | $2,622 | 611 | - | - | $4,485 54,513 kWh |
$2,622 611 MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |