Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Massachusetts |
---|---|
Assessment Year | 1998 |
Principal Product | Custom glass to metal sealing, soldering and brazing |
NAICS | n/a |
SIC | 3679 - Electronic Components, Nec |
Sales | $5,000,000-$10,000,000 |
# of Employees | 60 |
Plant Area (Sq.Ft.) | 14,280 |
Annual Production | 3,000,000 Pieces |
Production Hrs. Annual | 2,375 |
Location (State) | NH |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $49,079 | 520,223 | kWh | $0.09 |
Electricity Demand | $12,254 | 1,648 | kW-months/year | $7.44 |
LPG | $8,329 | 930 | MMBtu | $8.96 |
TOTAL ENERGY COSTS | $80,245 | |||
RECOMMENDED SAVINGS* | $16,338 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $3,784 |
#|Description |
Savings Cost |
Status | Electricity Usage | Electricity Demand | LPG | Gaseous Waste | By-product Production | Electricity Usage | Electricity Demand | LPG | Gaseous Waste | By-product Production | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | kW-months/year | $ | MMBtu | $ | lb | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4222 INSTALL ADEQUATE DRYERS ON AIR LINES TO ELIMINATE BLOWDOWN |
Savings: $1,280 Cost: $2,110 |
$(-81) | (-879) | $(-34) | (-4) | - | - | $1,395 | 124,693 | - | - |
$(-81) (-879) kWh |
$(-34) (-4) kW-months/year |
- - MMBtu |
$1,395 124,693 lb |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $642 Cost: $30 |
$437 | 4,689 | $205 | 24 | - | - | - | - | - | - |
$437 4,689 kWh |
$205 24 kW-months/year |
- - MMBtu |
- - lb |
- - $ |
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03: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT |
Savings: $3,142 Cost: $980 |
$(-54) | (-586) | $(-17) | (-2) | $3,213 | 359 | - | - | - | - |
$(-54) (-586) kWh |
$(-17) (-2) kW-months/year |
$3,213 359 MMBtu |
- - lb |
- - $ |
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04: 4.424 IMPROVE SPACE COMFORT CONDITIONING |
Savings: $5,656 Cost: $11,874 |
$(-189) | (-2,052) | $(-316) | (-37) | - | - | - | - | $6,161 | - |
$(-189) (-2,052) kWh |
$(-316) (-37) kW-months/year |
- - MMBtu |
- - lb |
$6,161 - $ |
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05: 4.212 ADOPT IN-HOUSE MATERIAL GENERATION |
Savings: $5,618 Cost: $29,750 |
$(-3,438) | (-37,222) | $(-1,527) | (-178) | - | - | $10,583 | 945,997 | - | - |
$(-3,438) (-37,222) kWh |
$(-1,527) (-178) kW-months/year |
- - MMBtu |
$10,583 945,997 lb |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $16,338 Cost: $44,744 |
$(-3,325) | (-36,050) | $(-1,689) | (-197) | $3,213 | 359 | $11,978 | 1,070,690 | $6,161 | - | $(-3,325) (-36,050) kWh |
$(-1,689) (-197) kW-months/year |
$3,213 359 MMBtu |
$11,978 1,070,690 lb |
$6,161 - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $3,784 Cost: $1,010 |
$383 | 4,103 | $188 | 22 | $3,213 | 359 | - | - | - | - | $383 4,103 kWh |
$188 22 kW-months/year |
$3,213 359 MMBtu |
- - lb |
- - $ |
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Savings Cost |
$ | kWh | $ | kW-months/year | $ | MMBtu | $ | lb | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Electricity Demand | LPG | Gaseous Waste | By-product Production | Electricity Usage | Electricity Demand | LPG | Gaseous Waste | By-product Production |