Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Massachusetts |
---|---|
Assessment Year | 2013 |
Principal Product | Rpair of Helicopter Parts |
NAICS | 336413 - Other Aircraft Parts and Auxiliary Equipment Manufacturing |
SIC | 3728 - Aircraft Parts And Equipment, Nec |
Sales | $50,000,000-$100,000,000 |
# of Employees | 200 |
Plant Area (Sq.Ft.) | 180,000 |
Annual Production | 4,560 Pieces |
Production Hrs. Annual | 5,406 |
Location (State) | CT |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $333,834 | 2,764,400 | kWh | $0.12 |
Electricity Demand | $102,784 | 7,380 | kW-months/year | $13.93 |
Electricity Fees | $4,116 | - | $ | - |
Natural Gas | $88,481 | 6,104 | MMBtu | $14.50 |
TOTAL ENERGY COSTS | $529,215 | |||
RECOMMENDED SAVINGS* | $49,273 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $30,225 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE |
Savings: $15,477 Cost: $1,400 |
- | - | - | - | $15,477 | - |
- - kWh |
- - MMBtu |
$15,477 - $ |
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02: 2.7224 REDUCE SPACE CONDITIONING DURING NON-WORKING HOURS |
Savings: $10,906 Cost: $7,500 |
$6,773 | 56,918 | $4,133 | 267 | - | - |
$6,773 56,918 kWh |
$4,133 267 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $7,493 Cost: $11,000 |
$7,493 | 60,916 | - | - | - | - |
$7,493 60,916 kWh |
- - MMBtu |
- - $ |
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04: 2.8121 APPLY FOR TAX-FREE STATUS FOR ENERGY PURCHASES |
Savings: $4,864 Cost: $200 |
- | - | - | - | $4,864 | - |
- - kWh |
- - MMBtu |
$4,864 - $ |
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05: 2.7221 LOWER TEMPERATURE DURING THE WINTER SEASON AND VICE-VERSA |
Savings: $2,474 Cost: $200 |
$1,143 | 9,603 | $1,331 | 86 | - | - |
$1,143 9,603 kWh |
$1,331 86 MMBtu |
- - $ |
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06: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $2,358 Cost: $1,120 |
$2,358 | 19,167 | - | - | - | - |
$2,358 19,167 kWh |
- - MMBtu |
- - $ |
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07: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $2,130 Cost: $1,020 |
$2,130 | 17,313 | - | - | - | - |
$2,130 17,313 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
08: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $2,106 Cost: $6,390 |
$2,106 | 17,118 | - | - | - | - |
$2,106 17,118 kWh |
- - MMBtu |
- - $ |
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09: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $1,465 Cost: $1,650 |
- | - | $1,465 | 101 | - | - |
- - kWh |
$1,465 101 MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $49,273 Cost: $30,480 |
$22,003 | 181,035 | $6,929 | 454 | $20,341 | - | $22,003 181,035 kWh |
$6,929 454 MMBtu |
$20,341 - $ |
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TOTAL IMPLEMENTED |
Savings: $30,225 Cost: $21,040 |
$19,897 | 163,917 | $5,464 | 353 | $4,864 | - | $19,897 163,917 kWh |
$5,464 353 MMBtu |
$4,864 - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |