Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Miami |
---|---|
Assessment Year | 2003 |
Principal Product | Automotive Body Repair and Paint Shop |
NAICS | 811118 - Other Automotive Mechanical and Electrical Repair and Maintenance |
SIC | 7539 - Automotive Repair Shops, Nec |
Sales | $5,000,000-$10,000,000 |
# of Employees | 65 |
Plant Area (Sq.Ft.) | 59,550 |
Annual Production | 0 Units |
Production Hrs. Annual | 4,160 |
Location (State) | FL |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $100,394 | 1,754,959 | kWh | $0.06 |
Electricity Demand | $30,583 | 4,346 | kW-months/year | $7.04 |
TOTAL ENERGY COSTS | $137,967 | |||
RECOMMENDED SAVINGS* | $38,834 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Administrative Changes | Electricity Usage | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE |
Savings: $12,419 Cost: - |
- | - | $12,419 | - |
- - kWh |
$12,419 - $ |
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02: 2.6218 TURN OFF EQUIPMENT WHEN NOT IN USE |
Savings: $19,897 Cost: $1,900 |
$19,897 | 455,686 | - | - |
$19,897 455,686 kWh |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $2,876 Cost: $4,556 |
$2,876 | 63,661 | - | - |
$2,876 63,661 kWh |
- - $ |
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04: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $207 Cost: $325 |
$207 | 4,586 | - | - |
$207 4,586 kWh |
- - $ |
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05: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $370 Cost: $85 |
$370 | 8,205 | - | - |
$370 8,205 kWh |
- - $ |
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06: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $42 Cost: $231 |
$42 | 929 | - | - |
$42 929 kWh |
- - $ |
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07: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $283 Cost: $244 |
$283 | 6,256 | - | - |
$283 6,256 kWh |
- - $ |
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08: 2.7232 REPLACE EXISTING HVAC UNIT WITH HIGH EFFICIENCY MODEL |
Savings: $2,740 Cost: $8,820 |
$2,740 | 60,642 | - | - |
$2,740 60,642 kWh |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $38,834 Cost: $16,161 |
$26,415 | 599,965 | $12,419 | - | $26,415 599,965 kWh |
$12,419 - $ |
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TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - - kWh |
- - $ |
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Savings Cost |
$ | kWh | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Administrative Changes | Electricity Usage | Administrative Changes |