Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Miami |
---|---|
Assessment Year | 2004 |
Principal Product | Women’s Sportswear |
NAICS | 315240 - Women’s, Girls’, and Infants’ Cut and Sew Apparel Manufacturing |
SIC | 2339 - Women's, Misses', and Juniors' Outerwear, Not Elsewhere Classified |
Sales | $10,000,000-$50,000,000 |
# of Employees | 100 |
Plant Area (Sq.Ft.) | 59,991 |
Annual Production | 300,000 Pieces |
Production Hrs. Annual | 2,210 |
Location (State) | FL |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $50,973 | 1,039,262 | kWh | $0.05 |
Electricity Demand | $29,254 | 4,305 | kW-months/year | $6.80 |
Electricity Fees | $16,445 | - | $ | - |
TOTAL ENERGY COSTS | $96,672 | |||
RECOMMENDED SAVINGS* | $68,484 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $61,540 |
#|Description |
Savings Cost |
Status | Electricity Usage | Administrative Changes | Electricity Usage | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE |
Savings: $4,105 Cost: $600 |
- | - | $4,105 | - |
- - kWh |
$4,105 - $ |
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02: 2.6218 TURN OFF EQUIPMENT WHEN NOT IN USE |
Savings: $5,344 Cost: $100 |
$5,344 | 112,164 | - | - |
$5,344 112,164 kWh |
- - $ |
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03: 4.322 ELIMINATE OLD STOCK AND MODIFY INVENTORY CONTROL |
Savings: $10,968 Cost: $5,200 |
- | - | $10,968 | - |
- - kWh |
$10,968 - $ |
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04: 2.2523 REDUCE INFILTRATION TO REFRIGERATED AREAS; ISOLATE HOT EQUIPMENT FROM REFRIGERATED AREAS |
Savings: $338 Cost: $354 |
$338 | 7,101 | - | - |
$338 7,101 kWh |
- - $ |
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05: 2.7447 INSTALL VINYL STRIP / HIGH SPEED / AIR CURTAIN DOORS |
Savings: $1,213 Cost: $1,200 |
$1,213 | 25,253 | - | - |
$1,213 25,253 kWh |
- - $ |
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06: 4.512 CONDENSE OPERATION INTO ONE BUILDING |
Savings: $44,015 Cost: $3,220 |
$9,015 | 92,161 | $35,000 | - |
$9,015 92,161 kWh |
$35,000 - $ |
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07: 2.7135 INSTALL OCCUPANCY SENSORS |
Savings: $133 Cost: $125 |
$133 | 4,738 | - | - |
$133 4,738 kWh |
- - $ |
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08: 2.7132 INSTALL TIMERS ON LIGHT SWITCHES IN LITTLE USED AREAS |
Savings: $2,368 Cost: $1,635 |
$2,368 | 511 | - | - |
$2,368 511 kWh |
- - $ |
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TOTAL RECOMMENDED |
Savings: $68,484 Cost: $12,434 |
$18,411 | 241,928 | $50,073 | - | $18,411 241,928 kWh |
$50,073 - $ |
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TOTAL IMPLEMENTED |
Savings: $61,540 Cost: $9,720 |
$15,572 | 229,578 | $45,968 | - | $15,572 229,578 kWh |
$45,968 - $ |
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Savings Cost |
$ | kWh | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Administrative Changes | Electricity Usage | Administrative Changes |