Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Miami |
---|---|
Assessment Year | 2004 |
Principal Product | Juice extraction, packaging and pellets |
NAICS | 311421 - Fruit and Vegetable Canning |
SIC | 2038 - Frozen Specialties, Nec |
Sales | $50,000,000-$100,000,000 |
# of Employees | 135 |
Plant Area (Sq.Ft.) | 254,800 |
Annual Production | 214,986 Tons |
Production Hrs. Annual | 8,760 |
Location (State) | FL |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $634,626 | 13,584,648 | kWh | $0.05 |
Electricity Demand | $238,810 | 29,746 | kW-months/year | $8.03 |
Electricity Fees | $11,992 | - | $ | - |
Fuel Oil #6 | $3,422,952 | 539,487 | MMBtu | $6.34 |
TOTAL ENERGY COSTS | $4,308,380 | |||
RECOMMENDED SAVINGS* | $370,405 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $138,625 |
#|Description |
Savings Cost |
Status | Electricity Usage | Fuel Oil #6 | Administrative Changes | Electricity Usage | Fuel Oil #6 | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE |
Savings: $21,521 Cost: $600 |
- | - | - | - | $21,521 | - |
- - kWh |
- - MMBtu |
$21,521 - $ |
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02: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $7,957 Cost: $1,649 |
- | - | $7,957 | 1,100 | - | - |
- - kWh |
$7,957 1,100 MMBtu |
- - $ |
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03: 2.1221 REPLACE OBSOLETE BURNERS WITH MORE EFFICIENT ONES |
Savings: $108,501 Cost: $33,050 |
- | - | $108,501 | 17,101 | - | - |
- - kWh |
$108,501 17,101 MMBtu |
- - $ |
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04: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $1,693 Cost: $250 |
$1,693 | 33,916 | - | - | - | - |
$1,693 33,916 kWh |
- - MMBtu |
- - $ |
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05: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $138,625 Cost: $68,380 |
- | - | $138,625 | 21,865 | - | - |
- - kWh |
$138,625 21,865 MMBtu |
- - $ |
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06: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $19,937 Cost: $61,795 |
$19,937 | 399,483 | - | - | - | - |
$19,937 399,483 kWh |
- - MMBtu |
- - $ |
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07: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $778 Cost: $178 |
$778 | 15,594 | - | - | - | - |
$778 15,594 kWh |
- - MMBtu |
- - $ |
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08: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $3,053 Cost: $450 |
- | - | $3,053 | 433 | - | - |
- - kWh |
$3,053 433 MMBtu |
- - $ |
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09: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $60,234 Cost: $5,408 |
- | - | $60,234 | 9,501 | - | - |
- - kWh |
$60,234 9,501 MMBtu |
- - $ |
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10: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $4,416 Cost: $2,670 |
$4,416 | 88,483 | - | - | - | - |
$4,416 88,483 kWh |
- - MMBtu |
- - $ |
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11: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $3,690 Cost: - |
$3,690 | 73,790 | - | - | - | - |
$3,690 73,790 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $370,405 Cost: $174,430 |
$30,514 | 611,266 | $318,370 | 50,000 | $21,521 | - | $30,514 611,266 kWh |
$318,370 50,000 MMBtu |
$21,521 - $ |
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TOTAL IMPLEMENTED |
Savings: $138,625 Cost: $68,380 |
- | - | $138,625 | 21,865 | - | - | - - kWh |
$138,625 21,865 MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Fuel Oil #6 | Administrative Changes | Electricity Usage | Fuel Oil #6 | Administrative Changes |