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IAC Assessment: MI0147
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IAC Assessment: MI0147
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IAC Center University of Miami
Assessment Year 2007
Principal Product Beef
NAICS 311611 - Animal (except Poultry) Slaughtering
SIC 2011 - Meat Packing Plants
Sales $10,000,000-$50,000,000
# of Employees 200
Plant Area (Sq.Ft.) 50,000
Annual Production 130,000 Units
Production Hrs. Annual 6,240
Location (State) FL
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $361,343 4,695,540 kWh $0.08
Electricity Demand $33,256 9,813 kW-months/year $3.39
Electricity Fees $32,470 - $ -
LPG $161,747 11,521 MMBtu $14.04
TOTAL ENERGY COSTS $588,816
RECOMMENDED SAVINGS* $45,815 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $41,384
#|Description Savings
Cost
Status Electricity Usage Electricity Demand Natural Gas LPG Electricity Usage Electricity Demand Natural Gas LPG
$ kWh $ kW-months/year $ MMBtu $ MMBtu
01: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT Savings:
$20,581
Cost:
$16,000
- - - - $20,581 1,468 - - -
-
kWh
-
-
kW-months/year
$20,581
1,468
MMBtu
-
-
MMBtu
02: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$10,498
Cost:
$1,750
- - - - - - $10,498 741 -
-
kWh
-
-
kW-months/year
-
-
MMBtu
$10,498
741
MMBtu
03: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$10,305
Cost:
$7,878
$9,326 208,546 $979 287 - - - - $9,326
208,546
kWh
$979
287
kW-months/year
-
-
MMBtu
-
-
MMBtu
04: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$3,950
Cost:
$1,074
$3,950 176,082 - - - - - - $3,950
176,082
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
MMBtu
05: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$481
Cost:
$30
$376 5,367 $105 644 - - - - $376
5,367
kWh
$105
644
kW-months/year
-
-
MMBtu
-
-
MMBtu
TOTAL RECOMMENDED Savings:
$45,815
Cost:
$26,732
$13,652 389,995 $1,084 931 $20,581 1,468 $10,498 741 $13,652
389,995
kWh
$1,084
931
kW-months/year
$20,581
1,468
MMBtu
$10,498
741
MMBtu
TOTAL IMPLEMENTED Savings:
$41,384
Cost:
$25,628
$9,326 208,546 $979 287 $20,581 1,468 $10,498 741 $9,326
208,546
kWh
$979
287
kW-months/year
$20,581
1,468
MMBtu
$10,498
741
MMBtu
Savings
Cost
$ kWh $ kW-months/year $ MMBtu $ MMBtu
Electricity Usage Electricity Demand Natural Gas LPG Electricity Usage Electricity Demand Natural Gas LPG