Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Mississippi State |
---|---|
Assessment Year | 1998 |
Principal Product | Pants |
NAICS | n/a |
SIC | 2325 - Men's and Boys' Separate Trousers and Slacks |
Sales | $50,000,000-$100,000,000 |
# of Employees | 119 |
Plant Area (Sq.Ft.) | 60,000 |
Annual Production | 5,000,000 Pieces |
Production Hrs. Annual | 2,500 |
Location (State) | AL |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $27,089 | 588,804 | kWh | $0.05 |
Electricity Demand | $17,064 | 3,600 | kW-months/year | $4.74 |
Electricity Fees | $10,063 | - | $ | - |
Natural Gas | $66,366 | 11,150 | MMBtu | $5.95 |
TOTAL ENERGY COSTS | $128,682 | |||
RECOMMENDED SAVINGS* | $28,292 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $9,961 |
#|Description |
Savings Cost |
Status | Electricity Usage | Electricity Demand | Natural Gas | Solid Waste (non-haz) | Administrative Changes | Ancillary Material Cost | Electricity Usage | Electricity Demand | Natural Gas | Solid Waste (non-haz) | Administrative Changes | Ancillary Material Cost | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | kW-months/year | $ | MMBtu | $ | lb | $ | $ | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $16,334 Cost: $5,000 |
- | - | - | - | $16,334 | 2,754 | - | - | - | - | - | - |
- - kWh |
- - kW-months/year |
$16,334 2,754 MMBtu |
- - lb |
- - $ |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.7229 AIR CONDITION ONLY SPACE NECESSARY |
Savings: $1,716 Cost: - |
- | - | - | - | $1,716 | 247 | - | - | - | - | - | - |
- - kWh |
- - kW-months/year |
$1,716 247 MMBtu |
- - lb |
- - $ |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.2153 CLOSE OFF UNNEEDED STEAM LINES |
Savings: $176 Cost: - |
- | - | - | - | $176 | 30 | - | - | - | - | - | - |
- - kWh |
- - kW-months/year |
$176 30 MMBtu |
- - lb |
- - $ |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
04: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $1,134 Cost: - |
$608 | 23,154 | $526 | 111 | - | - | - | - | - | - | - | - |
$608 23,154 kWh |
$526 111 kW-months/year |
- - MMBtu |
- - lb |
- - $ |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
05: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE |
Savings: $2,285 Cost: - |
- | - | $2,285 | - | - | - | - | - | - | - | - | - |
- - kWh |
$2,285 - kW-months/year |
- - MMBtu |
- - lb |
- - $ |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
06: 3.1162 USE LESS WASTEFUL PACKAGING |
Savings: $1,997 Cost: $34,896 |
- | - | - | - | - | - | $(-12,000) | 24,000 | - | - | $13,997 | - |
- - kWh |
- - kW-months/year |
- - MMBtu |
$(-12,000) 24,000 lb |
- - $ |
$13,997 - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
07: 4.522 MODIFY STORAGE SPACE TO AVOID RENTAL OF A WAREHOUSE |
Savings: $4,650 Cost: $5,000 |
- | - | - | - | - | - | - | - | $4,650 | - | - | - |
- - kWh |
- - kW-months/year |
- - MMBtu |
- - lb |
$4,650 - $ |
- - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $28,292 Cost: $44,896 |
$608 | 23,154 | $2,811 | 111 | $18,226 | 3,031 | $(-12,000) | 24,000 | $4,650 | - | $13,997 | - | $608 23,154 kWh |
$2,811 111 kW-months/year |
$18,226 3,031 MMBtu |
$(-12,000) 24,000 lb |
$4,650 - $ |
$13,997 - $ |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $9,961 Cost: $5,000 |
$608 | 23,154 | $2,811 | 111 | $1,892 | 277 | - | - | $4,650 | - | - | - | $608 23,154 kWh |
$2,811 111 kW-months/year |
$1,892 277 MMBtu |
- - lb |
$4,650 - $ |
- - $ |
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Savings Cost |
$ | kWh | $ | kW-months/year | $ | MMBtu | $ | lb | $ | $ | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Electricity Demand | Natural Gas | Solid Waste (non-haz) | Administrative Changes | Ancillary Material Cost | Electricity Usage | Electricity Demand | Natural Gas | Solid Waste (non-haz) | Administrative Changes | Ancillary Material Cost |