Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Mississippi State |
---|---|
Assessment Year | 2008 |
Principal Product | Pigment |
NAICS | 325130 - Synthetic Dye and Pigment Manufacturing |
SIC | 2861 - Gum And Wood Chemicals |
Sales | >$500,000,000 |
# of Employees | 400 |
Plant Area (Sq.Ft.) | 3,267,000 |
Annual Production | 225,000 Tons |
Production Hrs. Annual | 8,760 |
Location (State) | MS |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $42,179,670 | 1,114,765,814 | kWh | $0.04 |
Natural Gas | $18,465,453 | 2,462,060 | MMBtu | $7.50 |
TOTAL ENERGY COSTS | $60,645,123 | |||
RECOMMENDED SAVINGS* | $1,144,045 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $1,095,334 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $1,062,600 Cost: $94 |
- | - | $1,062,600 | 139,586 |
- - kWh |
$1,062,600 139,586 MMBtu |
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02: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $48,711 Cost: $29,850 |
$48,711 | 1,353,096 | - | - |
$48,711 1,353,096 kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $18,624 Cost: $376 |
$18,624 | 517,337 | - | - |
$18,624 517,337 kWh |
- - MMBtu |
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04: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $14,110 Cost: $500 |
- | - | $14,110 | 1,881 |
- - kWh |
$14,110 1,881 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $1,144,045 Cost: $30,820 |
$67,335 | 1,870,433 | $1,076,710 | 141,467 | $67,335 1,870,433 kWh |
$1,076,710 141,467 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $1,095,334 Cost: $970 |
$18,624 | 517,337 | $1,076,710 | 141,467 | $18,624 517,337 kWh |
$1,076,710 141,467 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |