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IAC Assessment: MZ0365
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IAC Assessment: MZ0365
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center University of Missouri-Columbia
Assessment Year 2024
Principal Product gas, electric and wood fireplace
NAICS 332510 - Hardware Manufacturing
SIC 3433 - Heating Equipment, Except Electric
Sales $100,000,000-$500,000,000
# of Employees 257
Plant Area (Sq.Ft.) 450,000
Annual Production 101,749 Pieces
Production Hrs. Annual 4,000
Location (State) IA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $276,008 6,445,500 kWh $0.04
Electricity Demand $407,629 20,685 kW-months/year $19.71
Natural Gas $172,475 44,634 MMBtu $3.86
TOTAL ENERGY COSTS $856,112
RECOMMENDED SAVINGS* $305,514 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Electricity Demand Natural Gas One-time Revenue or Avoided Cost Electricity Usage Electricity Demand Natural Gas One-time Revenue or Avoided Cost
$ kWh $ kW-months/year $ MMBtu $ $
01: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$6,949
Cost:
$1,000
$2,928 68,088 $4,021 204 - - - - $2,928
68,088
kWh
$4,021
204
kW-months/year
-
-
MMBtu
-
-
$
02: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$17,558
Cost:
$75,320
$17,558 408,329 - - - - - - $17,558
408,329
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
$
03: 2.4239 ELIMINATE OR REDUCE COMPRESSED AIR USAGE Savings:
$3,741
Cost:
$805
$154 3,575 $3,587 182 - - - - $154
3,575
kWh
$3,587
182
kW-months/year
-
-
MMBtu
-
-
$
04: 2.7124 MAKE A PRACTICE OF TURNING OFF LIGHTS WHEN NOT NEEDED Savings:
$96
Cost:
$520
$96 2,232 - - - - - - $96
2,232
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
$
05: 2.2622 REPLACE EXISTING CHILLER WITH HIGH EFFICIENCY MODEL Savings:
$267,134
Cost:
$875,396
$37,821 879,564 $45,313 2,299 - - $184,000 - $37,821
879,564
kWh
$45,313
2,299
kW-months/year
-
-
MMBtu
$184,000
-
$
06: 2.6231 UTILIZE CONTROLS TO OPERATE EQUIPMENT ONLY WHEN NEEDED Savings:
$10,036
Cost:
$6,500
- - - - $10,036 2,600 - - -
-
kWh
-
-
kW-months/year
$10,036
2,600
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$305,514
Cost:
$959,541
$58,557 1,361,788 $52,921 2,685 $10,036 2,600 $184,000 - $58,557
1,361,788
kWh
$52,921
2,685
kW-months/year
$10,036
2,600
MMBtu
$184,000
-
$
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - - - -
-
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
$
Savings
Cost
$ kWh $ kW-months/year $ MMBtu $ $
Electricity Usage Electricity Demand Natural Gas One-time Revenue or Avoided Cost Electricity Usage Electricity Demand Natural Gas One-time Revenue or Avoided Cost