Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Nebraska–Lincoln |
---|---|
Assessment Year | 2022 |
Principal Product | Treated Wastewater |
NAICS | 221320 - Sewage Treatment Facilities |
SIC | 4952 - Sewerage Systems |
Sales | $1,000,000-$5,000,000 |
# of Employees | 7 |
Plant Area (Sq.Ft.) | 300,000 |
Annual Production | 584,000 Thousand Gallons |
Production Hrs. Annual | 8,760 |
Location (State) | MN |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $93,986 | 1,592,983 | kWh | $0.06 |
Electricity Demand | $24,827 | 1,439 | kW-months/year | $17.25 |
Natural Gas | $99,142 | 10,312 | MMBtu | $9.61 |
TOTAL ENERGY COSTS | $262,344 | |||
RECOMMENDED SAVINGS* | $30,908 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $25,670 |
#|Description |
Savings Cost |
Status | Electricity Usage | Electricity Demand | Natural Gas | Solid Waste (non-haz) | Personnel Changes | Electricity Usage | Electricity Demand | Natural Gas | Solid Waste (non-haz) | Personnel Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | kW-months/year | $ | MMBtu | $ | lb | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4323 USE OPTIMUM SIZE AND CAPACITY EQUIPMENT |
Savings: $16,217 Cost: $225,000 |
$11,580 | 196,224 | $4,637 | 269 | - | - | - | - | - | - |
$11,580 196,224 kWh |
$4,637 269 kW-months/year |
- - MMBtu |
- - lb |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.6231 UTILIZE CONTROLS TO OPERATE EQUIPMENT ONLY WHEN NEEDED |
Savings: $7,537 Cost: $35,000 |
$1,106 | 18,746 | $443 | 26 | - | - | - | - | $5,988 | - |
$1,106 18,746 kWh |
$443 26 kW-months/year |
- - MMBtu |
- - lb |
$5,988 - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES |
Savings: $5,239 Cost: $1,398 |
$(-382) | (-6,481) | $5,621 | 381 | - | - | - | - | - | - |
$(-382) (-6,481) kWh |
$5,621 381 kW-months/year |
- - MMBtu |
- - lb |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
04: 3.3133 USE OTHER WASTE CONCENTRATION METHODS |
Savings: $1,144 Cost: $1,258 |
- | - | - | - | $(-1,075) | (-112) | $2,219 | 24,660 | - | - |
- - kWh |
- - kW-months/year |
$(-1,075) (-112) MMBtu |
$2,219 24,660 lb |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
05: 2.4239 ELIMINATE OR REDUCE COMPRESSED AIR USAGE |
Savings: $772 Cost: $58 |
- | - | $772 | 45 | - | - | - | - | - | - |
- - kWh |
$772 45 kW-months/year |
- - MMBtu |
- - lb |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $30,908 Cost: $262,714 |
$12,304 | 208,489 | $11,473 | 720 | $(-1,075) | (-112) | $2,219 | 24,660 | $5,988 | - | $12,304 208,489 kWh |
$11,473 720 kW-months/year |
$(-1,075) (-112) MMBtu |
$2,219 24,660 lb |
$5,988 - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $25,670 Cost: $261,316 |
$12,686 | 214,970 | $5,852 | 339 | $(-1,075) | (-112) | $2,219 | 24,660 | $5,988 | - | $12,686 214,970 kWh |
$5,852 339 kW-months/year |
$(-1,075) (-112) MMBtu |
$2,219 24,660 lb |
$5,988 - $ |
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Savings Cost |
$ | kWh | $ | kW-months/year | $ | MMBtu | $ | lb | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Electricity Demand | Natural Gas | Solid Waste (non-haz) | Personnel Changes | Electricity Usage | Electricity Demand | Natural Gas | Solid Waste (non-haz) | Personnel Changes |