Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Oklahoma State University |
---|---|
Assessment Year | 2000 |
Principal Product | Prefabricated piping systems |
NAICS | n/a |
SIC | 3498 - Fabricated Pipe And Fittings |
Sales | $10,000,000-$50,000,000 |
# of Employees | 250 |
Plant Area (Sq.Ft.) | 100,000 |
Annual Production | 8,100 Tons |
Production Hrs. Annual | 2,574 |
Location (State) | OK |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $123,951 | 2,691,090 | kWh | $0.05 |
Electricity Fees | $2,934 | - | $ | - |
Natural Gas | $62,517 | 23,817 | MMBtu | $2.62 |
TOTAL ENERGY COSTS | $495,757 | |||
RECOMMENDED SAVINGS* | $542,301 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | - |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Personnel Changes | Administrative Changes | Ancillary Material Cost | Electricity Usage | Natural Gas | Personnel Changes | Administrative Changes | Ancillary Material Cost | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | $ | $ | $ | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.8112 COMBINE UTILITY METERS |
Savings: $15,427 Cost: $10,600 |
- | - | - | - | - | - | $15,427 | - | - | - |
- - kWh |
- - MMBtu |
- - $ |
$15,427 - $ |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.7135 INSTALL OCCUPANCY SENSORS |
Savings: $777 Cost: $3,841 |
$777 | 16,413 | - | - | - | - | - | - | - | - |
$777 16,413 kWh |
- - MMBtu |
- - $ |
- - $ |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $6,866 Cost: $1,300 |
$6,866 | 166,764 | - | - | - | - | - | - | - | - |
$6,866 166,764 kWh |
- - MMBtu |
- - $ |
- - $ |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
04: 2.2442 PREHEAT COMBUSTION AIR WITH WASTE HEAT |
Savings: $6,139 Cost: $12,800 |
- | - | $6,139 | 1,709 | - | - | - | - | - | - |
- - kWh |
$6,139 1,709 MMBtu |
- - $ |
- - $ |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
05: 3.5311 RECOVER AND REUSE WASTE MATERIAL |
Savings: $89,040 Cost: - |
- | - | - | - | - | - | - | - | $89,040 | - |
- - kWh |
- - MMBtu |
- - $ |
- - $ |
$89,040 - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
06: 4.112 REPLACE OLD MACHINE WITH NEW AUTOMATIC MULTI-STATION TOOL |
Savings: $200,000 Cost: $300,000 |
- | - | - | - | $200,000 | - | - | - | - | - |
- - kWh |
- - MMBtu |
$200,000 - $ |
- - $ |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
07: 4.214 PURCHASE APPROPRIATELY SIZED MATERIAL |
Savings: $224,052 Cost: $150 |
- | - | - | - | $224,052 | - | - | - | - | - |
- - kWh |
- - MMBtu |
$224,052 - $ |
- - $ |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $542,301 Cost: $328,691 |
$7,643 | 183,177 | $6,139 | 1,709 | $424,052 | - | $15,427 | - | $89,040 | - | $7,643 183,177 kWh |
$6,139 1,709 MMBtu |
$424,052 - $ |
$15,427 - $ |
$89,040 - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: - Cost: - |
- | - | - | - | - | - | - | - | - | - | - - kWh |
- - MMBtu |
- - $ |
- - $ |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | $ | $ | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Personnel Changes | Administrative Changes | Ancillary Material Cost | Electricity Usage | Natural Gas | Personnel Changes | Administrative Changes | Ancillary Material Cost |