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IAC Assessment: OK0681
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IAC Assessment: OK0681
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Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
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IAC Center Oklahoma State University
Assessment Year 2004
Principal Product Plastic Cups and Plates
NAICS 326199 - All Other Plastics Product Manufacturing
SIC 3089 - Plastics Products, Nec
Sales $50,000,000-$100,000,000
# of Employees 120
Plant Area (Sq.Ft.) 176,800
Annual Production 6,800,000 Pieces
Production Hrs. Annual 8,000
Location (State) OK
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $981,377 26,641,599 kWh $0.04
Natural Gas $25,433 3,603 MMBtu $7.06
TOTAL ENERGY COSTS $1,014,970
RECOMMENDED SAVINGS* $415,881 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Personnel Changes Ancillary Material Cost Electricity Usage Personnel Changes Ancillary Material Cost
$ kWh $ $ $ $
01: 2.4224 UPGRADE CONTROLS ON COMPRESSORS Savings:
$19,254
Cost:
$25,000
$19,254 523,200 - - - - $19,254
523,200
kWh
-
-
$
-
-
$
02: 2.4227 USE COMPRESSOR AIR FILTERS Savings:
$4,163
Cost:
$130
$4,611 125,304 - - $(-448) - $4,611
125,304
kWh
-
-
$
$(-448)
-
$
03: 2.2625 CHILL WATER TO THE HIGHEST TEMPERATURE POSSIBLE Savings:
$10,131
Cost:
$11,350
$10,131 275,309 - - - - $10,131
275,309
kWh
-
-
$
-
-
$
04: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$3,342
Cost:
$10,540
$3,342 90,817 - - - - $3,342
90,817
kWh
-
-
$
-
-
$
05: 4.426 MODIFY WORKLOAD Savings:
$378,991
Cost:
$200,000
$48,991 1,331,287 $330,000 - - - $48,991
1,331,287
kWh
$330,000
-
$
-
-
$
TOTAL RECOMMENDED Savings:
$415,881
Cost:
$247,020
$86,329 2,345,917 $330,000 - $(-448) - $86,329
2,345,917
kWh
$330,000
-
$
$(-448)
-
$
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - -
-
kWh
-
-
$
-
-
$
Savings
Cost
$ kWh $ $ $ $
Electricity Usage Personnel Changes Ancillary Material Cost Electricity Usage Personnel Changes Ancillary Material Cost