IAC logo
IAC Assessment: OK0814
Sponsored by:
DOE MESC
IAC logo
IAC Assessment: OK0814
Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center Oklahoma State University
Assessment Year 2011
Principal Product Couplings and adapters
NAICS 332510 - Hardware Manufacturing
SIC 3429 - Hardware, Nec
Sales $50,000,000-$100,000,000
# of Employees 212
Plant Area (Sq.Ft.) 140,117
Annual Production 1,831 Tons
Production Hrs. Annual 2,600
Location (State) OK
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $434,646 6,068,480 kWh $0.07
Natural Gas $130,245 22,656 MMBtu $5.75
TOTAL ENERGY COSTS $564,891
RECOMMENDED SAVINGS* $1,845,816 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $1,822,703
#|Description Savings
Cost
Status Electricity Usage Natural Gas Personnel Changes Electricity Usage Natural Gas Personnel Changes
$ kWh $ MMBtu $ $
01: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES Savings:
$262,832
Cost:
$1,710,000
$20,142 281,320 - - $242,690 - $20,142
281,320
kWh
-
-
MMBtu
$242,690
-
$
02: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES Savings:
$189,220
Cost:
$20,000
$7,220 100,838 - - $182,000 - $7,220
100,838
kWh
-
-
MMBtu
$182,000
-
$
03: 4.445 INSTALL EQUIPMENT TO MOVE PRODUCT Savings:
$1,364,602
Cost:
$235,960
$(-7,846) (-109,587) - - $1,372,448 - $(-7,846)
(-109,587)
kWh
-
-
MMBtu
$1,372,448
-
$
04: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$6,049
Cost:
$15,319
$6,049 84,489 - - - - $6,049
84,489
kWh
-
-
MMBtu
-
-
$
05: 2.1133 ADJUST BURNERS FOR EFFICIENT OPERATION Savings:
$23,113
Cost:
$11,400
- - $23,113 4,020 - - -
-
kWh
$23,113
4,020
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$1,845,816
Cost:
$1,992,679
$25,565 357,060 $23,113 4,020 $1,797,138 - $25,565
357,060
kWh
$23,113
4,020
MMBtu
$1,797,138
-
$
TOTAL IMPLEMENTED Savings:
$1,822,703
Cost:
$1,981,279
$25,565 357,060 - - $1,797,138 - $25,565
357,060
kWh
-
-
MMBtu
$1,797,138
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Personnel Changes Electricity Usage Natural Gas Personnel Changes