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IAC Assessment: OR0056
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IAC Assessment: OR0056
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IAC Center Oregon State University
Assessment Year 1989
Principal Product SALADS,VEGGIES,SOUR CRM.
NAICS n/a
SIC 2099 - Food Preparations, Nec
Sales $10,000,000-$50,000,000
# of Employees 250
Plant Area (Sq.Ft.) 0
Annual Production 52,800,000 Pounds
Production Hrs. Annual 6,552
Location (State) OR
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $124,982 2,599,062 kWh $0.05
Natural Gas $106,495 23,453 MMBtu $4.54
TOTAL ENERGY COSTS $231,477
RECOMMENDED SAVINGS* $12,764 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $12,093
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE Savings:
$252
Cost:
-
$252 5,275 - - - - $252
5,275
kWh
-
-
MMBtu
-
-
$
02: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$2,873
Cost:
$100
- - $2,873 633 - - -
-
kWh
$2,873
633
MMBtu
-
-
$
03: 3.4151 MINIMIZE WATER USAGE Savings:
$3,946
Cost:
$1,683
- - - - $3,946 - -
-
kWh
-
-
MMBtu
$3,946
-
$
04: 2.1232 KEEP BOILER TUBES CLEAN Savings:
$1,821
Cost:
$100
- - $1,821 401 - - -
-
kWh
$1,821
401
MMBtu
-
-
$
05: 2.1213 DIRECT WARMEST AIR TO COMBUSTION INTAKE Savings:
$377
Cost:
$310
- - $377 83 - - -
-
kWh
$377
83
MMBtu
-
-
$
06: 2.2441 PREHEAT BOILER MAKEUP WATER WITH WASTE PROCESS HEAT Savings:
$3,201
Cost:
$2,750
- - $3,201 705 - - -
-
kWh
$3,201
705
MMBtu
-
-
$
07: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$294
Cost:
$750
$294 - - - - - $294
-
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$12,764
Cost:
$5,693
$546 5,275 $8,272 1,822 $3,946 - $546
5,275
kWh
$8,272
1,822
MMBtu
$3,946
-
$
TOTAL IMPLEMENTED Savings:
$12,093
Cost:
$4,633
$252 5,275 $7,895 1,739 $3,946 - $252
5,275
kWh
$7,895
1,739
MMBtu
$3,946
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes