Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Tennessee |
---|---|
Assessment Year | 1986 |
Principal Product | HVAC FILTER ENCLOSURES |
NAICS | n/a |
SIC | 3564 - Blowers And Fans |
Sales | $10,000,000-$50,000,000 |
# of Employees | 180 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 100,000 Pieces |
Production Hrs. Annual | 5,880 |
Location (State) | TN |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $122,884 | 2,432,005 | kWh | $0.05 |
Natural Gas | $55,381 | 10,290 | MMBtu | $5.38 |
TOTAL ENERGY COSTS | $178,265 | |||
RECOMMENDED SAVINGS* | $13,822 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $13,000 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $8,871 Cost: $4,270 |
$8,871 | 175,557 | - | - | - | - |
$8,871 175,557 kWh |
- - MMBtu |
- - $ |
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02: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $556 Cost: - |
- | - | $1,356 | 252 | $(-800) | - |
- - kWh |
$1,356 252 MMBtu |
$(-800) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $2,088 Cost: $165 |
$2,088 | 41,325 | - | - | - | - |
$2,088 41,325 kWh |
- - MMBtu |
- - $ |
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04: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $889 Cost: - |
$889 | 17,585 | - | - | - | - |
$889 17,585 kWh |
- - MMBtu |
- - $ |
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05: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS |
Savings: $822 Cost: $540 |
$822 | 16,120 | - | - | - | - |
$822 16,120 kWh |
- - MMBtu |
- - $ |
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06: 2.4227 USE COMPRESSOR AIR FILTERS |
Savings: $285 Cost: - |
$385 | 7,620 | - | - | $(-100) | - |
$385 7,620 kWh |
- - MMBtu |
$(-100) - $ |
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07: 2.6121 REDUCE HOT WATER TEMPERATURE TO THE MINIMUM REQUIRED |
Savings: $311 Cost: - |
$311 | 6,155 | - | - | - | - |
$311 6,155 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $13,822 Cost: $4,975 |
$13,366 | 264,362 | $1,356 | 252 | $(-900) | - | $13,366 264,362 kWh |
$1,356 252 MMBtu |
$(-900) - $ |
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TOTAL IMPLEMENTED |
Savings: $13,000 Cost: $4,435 |
$12,544 | 248,242 | $1,356 | 252 | $(-900) | - | $12,544 248,242 kWh |
$1,356 252 MMBtu |
$(-900) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |