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IAC Assessment: TN0363
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IAC Assessment: TN0363
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IAC Center University of Tennessee
Assessment Year 1989
Principal Product PRESSED GLASSWARE
NAICS n/a
SIC 3229 - Pressed And Blown Glass, Nec
Sales $10,000,000-$50,000,000
# of Employees 235
Plant Area (Sq.Ft.) 0
Annual Production 93,000,000 Pieces
Production Hrs. Annual 7,896
Location (State) KY
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $936,989 27,509,965 kWh $0.03
Natural Gas $1,474,272 415,988 MMBtu $3.54
TOTAL ENERGY COSTS $2,411,261
RECOMMENDED SAVINGS* $213,825 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $213,825
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$125,794
Cost:
$1,200
- - $125,794 35,941 - - -
-
kWh
$125,794
35,941
MMBtu
-
-
$
02: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT Savings:
$57,307
Cost:
$379,000
- - $57,307 16,373 - - -
-
kWh
$57,307
16,373
MMBtu
-
-
$
03: 2.2111 INSTALL STEAM TRAP Savings:
$8,302
Cost:
$3,450
- - $8,302 2,372 - - -
-
kWh
$8,302
2,372
MMBtu
-
-
$
04: 2.2163 USE MINIMUM STEAM OPERATING PRESSURE Savings:
$3,504
Cost:
-
- - $3,504 1,001 - - -
-
kWh
$3,504
1,001
MMBtu
-
-
$
05: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$8,789
Cost:
$7,480
$8,789 258,499 - - - - $8,789
258,499
kWh
-
-
MMBtu
-
-
$
06: 2.7123 KEEP LAMPS AND REFLECTORS CLEAN Savings:
$6,829
Cost:
$21,293
$6,607 194,314 - - $222 - $6,607
194,314
kWh
-
-
MMBtu
$222
-
$
07: 2.6232 INSTALL SET-BACK TIMERS Savings:
$2,215
Cost:
-
$2,215 65,064 - - - - $2,215
65,064
kWh
-
-
MMBtu
-
-
$
08: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$1,085
Cost:
$600
- - $1,085 310 - - -
-
kWh
$1,085
310
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$213,825
Cost:
$413,023
$17,611 517,877 $195,992 55,997 $222 - $17,611
517,877
kWh
$195,992
55,997
MMBtu
$222
-
$
TOTAL IMPLEMENTED Savings:
$213,825
Cost:
$413,023
$17,611 517,877 $195,992 55,997 $222 - $17,611
517,877
kWh
$195,992
55,997
MMBtu
$222
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes