Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Dayton |
---|---|
Assessment Year | 1986 |
Principal Product | INJEC-MOLDED AUTO PARTS |
NAICS | n/a |
SIC | 3089 - Plastics Products, Nec |
Sales | $5,000,000-$10,000,000 |
# of Employees | 90 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 20,000,000 Pieces |
Production Hrs. Annual | 6,600 |
Location (State) | OH |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $108,907 | 1,966,002 | kWh | $0.06 |
TOTAL ENERGY COSTS | $108,907 | |||
RECOMMENDED SAVINGS* | $5,407 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $5,407 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT |
Savings: $1,234 Cost: $2,500 |
$1,884 | 29,894 | $(-650) | (-120) |
$1,884 29,894 kWh |
$(-650) (-120) MMBtu |
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02: 2.7314 REDUCE VENTILATION AIR |
Savings: $4,173 Cost: $2,500 |
$4,476 | 102,286 | $(-303) | (-56) |
$4,476 102,286 kWh |
$(-303) (-56) MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $5,407 Cost: $5,000 |
$6,360 | 132,180 | $(-953) | (-176) | $6,360 132,180 kWh |
$(-953) (-176) MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $5,407 Cost: $5,000 |
$6,360 | 132,180 | $(-953) | (-176) | $6,360 132,180 kWh |
$(-953) (-176) MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |