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IAC Assessment: UM0157
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IAC Assessment: UM0157
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IAC Center University of Michigan
Assessment Year 2000
Principal Product Linen and Garments
NAICS n/a
SIC 2389 - Apparel And Accessories, Nec
Sales $1,000,000-$5,000,000
# of Employees 30
Plant Area (Sq.Ft.) 22,000
Annual Production 12,000,000 Pounds
Production Hrs. Annual 4,680
Location (State) MI
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $65,806 716,295 kWh $0.09
Electricity Demand $4,126 352 kW-months/year $11.72
Electricity Fees $4,841 - $ -
Natural Gas $57,782 23,318 MMBtu $2.48
TOTAL ENERGY COSTS $132,555
RECOMMENDED SAVINGS* $12,427 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $4,427
#|Description Savings
Cost
Status Electricity Usage Electricity Demand Natural Gas Solid Waste (non-haz) Primary Product Electricity Usage Electricity Demand Natural Gas Solid Waste (non-haz) Primary Product
$ kWh $ kW-months/year $ MMBtu $ lb $ $
01: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$1,161
Cost:
$150
$758 12,896 $403 32 - - - - - - $758
12,896
kWh
$403
32
kW-months/year
-
-
MMBtu
-
-
lb
-
-
$
02: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS Savings:
$746
Cost:
$500
$746 7,034 - - - - - - - - $746
7,034
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
lb
-
-
$
03: 2.1241 REDUCE EXCESSIVE BOILER BLOWDOWN Savings:
$1,224
Cost:
$4,430
- - - - $1,224 493 - - - - -
-
kWh
-
-
kW-months/year
$1,224
493
MMBtu
-
-
lb
-
-
$
04: 3.5212 REGRIND, REUSE, OR SELL SCRAP PLASTIC PARTS Savings:
$8,000
Cost:
$400
- - - - - - $8,000 121,003,447 - - -
-
kWh
-
-
kW-months/year
-
-
MMBtu
$8,000
121,003,447
lb
-
-
$
05: 4.111 ADD EQUIPMENT/ OPERATORS TO REDUCE PRODUCTION BOTTLENECK Savings:
$1,296
Cost:
$738
- - - - - - - - $1,296 - -
-
kWh
-
-
kW-months/year
-
-
MMBtu
-
-
lb
$1,296
-
$
TOTAL RECOMMENDED Savings:
$12,427
Cost:
$6,218
$1,504 19,930 $403 32 $1,224 493 $8,000 121,003,447 $1,296 - $1,504
19,930
kWh
$403
32
kW-months/year
$1,224
493
MMBtu
$8,000
121,003,447
lb
$1,296
-
$
TOTAL IMPLEMENTED Savings:
$4,427
Cost:
$5,818
$1,504 19,930 $403 32 $1,224 493 - - $1,296 - $1,504
19,930
kWh
$403
32
kW-months/year
$1,224
493
MMBtu
-
-
lb
$1,296
-
$
Savings
Cost
$ kWh $ kW-months/year $ MMBtu $ lb $ $
Electricity Usage Electricity Demand Natural Gas Solid Waste (non-haz) Primary Product Electricity Usage Electricity Demand Natural Gas Solid Waste (non-haz) Primary Product