Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Texas A&M, College Station |
---|---|
Assessment Year | 1988 |
Principal Product | MANUFACTURED HOUSING |
NAICS | n/a |
SIC | 2451 - Mobile Homes |
Sales | $10,000,000-$50,000,000 |
# of Employees | 104 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 750 Pieces |
Production Hrs. Annual | 2,000 |
Location (State) | TX |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $36,465 | 519,637 | kWh | $0.07 |
Natural Gas | $1,544 | 412 | MMBtu | $3.75 |
TOTAL ENERGY COSTS | $38,009 | |||
RECOMMENDED SAVINGS* | $3,289 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $2,484 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $520 Cost: $188 |
$520 | 6,741 | - | - |
$520 6,741 kWh |
- - MMBtu |
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02: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $1,120 Cost: $500 |
$1,120 | 16,413 | - | - |
$1,120 16,413 kWh |
- - MMBtu |
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03: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $600 Cost: $300 |
$600 | 12,016 | - | - |
$600 12,016 kWh |
- - MMBtu |
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04: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT |
Savings: $340 Cost: $550 |
- | - | $340 | 90 |
- - kWh |
$340 90 MMBtu |
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05: 2.2443 RE-USE OR RECYCLE HOT OR COLD PROCESS EXHAUST AIR |
Savings: $300 Cost: $600 |
$300 | 2,345 | - | - |
$300 2,345 kWh |
- - MMBtu |
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06: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $210 Cost: - |
$210 | 4,103 | - | - |
$210 4,103 kWh |
- - MMBtu |
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07: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE |
Savings: $165 Cost: $625 |
$165 | 3,224 | - | - |
$165 3,224 kWh |
- - MMBtu |
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08: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $34 Cost: $100 |
$34 | 586 | - | - |
$34 586 kWh |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $3,289 Cost: $2,863 |
$2,949 | 45,428 | $340 | 90 | $2,949 45,428 kWh |
$340 90 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $2,484 Cost: $1,088 |
$2,484 | 39,859 | - | - | $2,484 39,859 kWh |
- - MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |