Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Texas A&M, College Station |
---|---|
Assessment Year | 1990 |
Principal Product | SOFT DRINKS |
NAICS | n/a |
SIC | 2086 - Bottled And Canned Soft Drinks |
Sales | $1,000,000-$5,000,000 |
# of Employees | 42 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 3,309,000 Pieces |
Production Hrs. Annual | 2,614 |
Location (State) | TX |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $115,293 | 1,657,093 | kWh | $0.07 |
Natural Gas | $25,677 | 4,977 | MMBtu | $5.16 |
TOTAL ENERGY COSTS | $140,970 | |||
RECOMMENDED SAVINGS* | $31,327 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $31,327 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT |
Savings: $15,000 Cost: $5,000 |
- | - | $15,000 | 2,800 |
- - kWh |
$15,000 2,800 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.3212 OPTIMIZE PLANT POWER FACTOR |
Savings: $7,969 Cost: $12,000 |
$7,969 | - | - | - |
$7,969 - kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $2,400 Cost: $540 |
- | - | $2,400 | 440 |
- - kWh |
$2,400 440 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
04: 2.4239 ELIMINATE OR REDUCE COMPRESSED AIR USAGE |
Savings: $2,000 Cost: $2,740 |
$2,000 | 46,893 | - | - |
$2,000 46,893 kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $1,930 Cost: $106 |
$1,930 | 44,842 | - | - |
$1,930 44,842 kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
06: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $900 Cost: - |
$900 | 12,309 | - | - |
$900 12,309 kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
07: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $270 Cost: $40 |
$270 | 3,810 | - | - |
$270 3,810 kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
08: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $488 Cost: $410 |
$488 | 11,430 | - | - |
$488 11,430 kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
09: 2.7133 USE SEPARATE SWITCHES ON PERIMETER LIGHTING WHICH MAY BE TURNED OFF WHEN NATURAL LIGHT IS AVAILABLE |
Savings: $370 Cost: $150 |
$370 | 5,275 | - | - |
$370 5,275 kWh |
- - MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $31,327 Cost: $20,986 |
$13,927 | 124,559 | $17,400 | 3,240 | $13,927 124,559 kWh |
$17,400 3,240 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $31,327 Cost: $20,986 |
$13,927 | 124,559 | $17,400 | 3,240 | $13,927 124,559 kWh |
$17,400 3,240 MMBtu |
||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |