Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Texas A&M, College Station |
---|---|
Assessment Year | 1994 |
Principal Product | Milk, chocolate milk, apple and orange juice, orange drink, |
NAICS | n/a |
SIC | 2026 - Fluid Milk |
Sales | $10,000,000-$50,000,000 |
# of Employees | 58 |
Plant Area (Sq.Ft.) | 47,800 |
Annual Production | 20,400 Thousand Gallons |
Production Hrs. Annual | 4,112 |
Location (State) | TX |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $283,041 | 5,603,752 | kWh | $0.05 |
Natural Gas | $36,419 | 9,267 | MMBtu | $3.93 |
TOTAL ENERGY COSTS | $319,460 | |||
RECOMMENDED SAVINGS* | $1,800 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $140 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Solid Waste (haz) | Electricity Usage | Natural Gas | Solid Waste (haz) | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | lb | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED |
Savings: $920 Cost: $3,180 |
- | - | $920 | 128 | - | - |
- - kWh |
$920 128 MMBtu |
- - lb |
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02: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED |
Savings: $550 Cost: $470 |
- | - | $550 | 73 | - | - |
- - kWh |
$550 73 MMBtu |
- - lb |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.7124 MAKE A PRACTICE OF TURNING OFF LIGHTS WHEN NOT NEEDED |
Savings: $140 Cost: - |
$140 | 5,275 | - | - | - | - |
$140 5,275 kWh |
- - MMBtu |
- - lb |
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04: 3.8132 USE LESS TOXIC AND VOLATILE SOLVENT SUBSTITUTES |
Savings: $190 Cost: $580 |
- | - | - | - | $190 | 1,150 |
- - kWh |
- - MMBtu |
$190 1,150 lb |
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TOTAL RECOMMENDED |
Savings: $1,800 Cost: $4,230 |
$140 | 5,275 | $1,470 | 201 | $190 | 1,150 | $140 5,275 kWh |
$1,470 201 MMBtu |
$190 1,150 lb |
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TOTAL IMPLEMENTED |
Savings: $140 Cost: - |
$140 | 5,275 | - | - | - | - | $140 5,275 kWh |
- - MMBtu |
- - lb |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | lb | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Solid Waste (haz) | Electricity Usage | Natural Gas | Solid Waste (haz) |