Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | University of Delaware |
---|---|
Assessment Year | 2012 |
Principal Product | Poultry Products |
NAICS | 311615 - Poultry Processing |
SIC | 2015 - Poultry Slaughtering And Processing |
Sales | $500,000-$1,000,000 |
# of Employees | 1,200 |
Plant Area (Sq.Ft.) | 162,962 |
Annual Production | 54,600,000 Pieces |
Production Hrs. Annual | 4,160 |
Location (State) | DE |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $2,575,902 | 27,897,000 | kWh | $0.09 |
Electricity Demand | $596,544 | 59,196 | kW-months/year | $10.08 |
Natural Gas | $711,488 | 99,616 | MMBtu | $7.14 |
LPG | $108,779 | 4,745 | MMBtu | $22.92 |
TOTAL ENERGY COSTS | $3,992,713 | |||
RECOMMENDED SAVINGS* | $584,732 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $152,843 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.4224 UPGRADE CONTROLS ON COMPRESSORS |
Savings: $323,076 Cost: $500,000 |
$323,076 | 2,834,000 | - | - |
$323,076 2,834,000 kWh |
- - MMBtu |
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02: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $51,870 Cost: $24,400 |
$51,870 | 455,000 | - | - |
$51,870 455,000 kWh |
- - MMBtu |
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03: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $33,801 Cost: $36,000 |
$33,801 | 296,500 | - | - |
$33,801 296,500 kWh |
- - MMBtu |
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04: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $40,818 Cost: $54,000 |
$40,818 | 358,059 | - | - |
$40,818 358,059 kWh |
- - MMBtu |
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05: 2.4222 INSTALL ADEQUATE DRYERS ON AIR LINES TO ELIMINATE BLOWDOWN |
Savings: $18,222 Cost: $42,000 |
$18,222 | 159,840 | - | - |
$18,222 159,840 kWh |
- - MMBtu |
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06: 2.6231 UTILIZE CONTROLS TO OPERATE EQUIPMENT ONLY WHEN NEEDED |
Savings: $24,850 Cost: $4,500 |
$24,850 | 217,981 | - | - |
$24,850 217,981 kWh |
- - MMBtu |
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07: 2.6231 UTILIZE CONTROLS TO OPERATE EQUIPMENT ONLY WHEN NEEDED |
Savings: $28,257 Cost: $28,000 |
$28,257 | 247,869 | - | - |
$28,257 247,869 kWh |
- - MMBtu |
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08: 2.1116 IMPROVE COMBUSTION CONTROL CAPABILITY |
Savings: $16,536 Cost: $8,900 |
- | - | $16,536 | 2,316 |
- - kWh |
$16,536 2,316 MMBtu |
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09: 2.1243 USE HEAT FROM BOILER BLOWDOWN TO PREHEAT BOILER FEED WATER |
Savings: $16,536 Cost: $25,000 |
- | - | $16,536 | 2,316 |
- - kWh |
$16,536 2,316 MMBtu |
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10: 2.7314 REDUCE VENTILATION AIR |
Savings: $26,354 Cost: $4,500 |
$26,354 | 231,175 | - | - |
$26,354 231,175 kWh |
- - MMBtu |
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11: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $4,412 Cost: $720 |
$4,412 | 38,700 | - | - |
$4,412 38,700 kWh |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $584,732 Cost: $728,020 |
$551,660 | 4,839,124 | $33,072 | 4,632 | $551,660 4,839,124 kWh |
$33,072 4,632 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $152,843 Cost: $118,900 |
$152,843 | 1,340,734 | - | - | $152,843 1,340,734 kWh |
- - MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |