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IAC Assessment: DL0114
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IAC Assessment: DL0114
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Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
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IAC Center University of Delaware
Assessment Year 2013
Principal Product Wire cloth, metal belting
NAICS 332618 - Other Fabricated Wire Product Manufacturing
SIC 3496 - Misc. Fabricated Wire Products
Sales $50,000,000-$100,000,000
# of Employees 50
Plant Area (Sq.Ft.) 346,000
Annual Production 9,999 Units
Production Hrs. Annual 6,000
Location (State) MD
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $346,133 5,069,553 kWh $0.07
Electricity Demand $68,457 12,758 kW-months/year $5.37
LPG $45,433 2,564 MMBtu $17.72
TOTAL ENERGY COSTS $460,023
RECOMMENDED SAVINGS* $118,501 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas LPG Electricity Usage Natural Gas LPG
$ kWh $ MMBtu $ MMBtu
01: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$7,410
Cost:
$2,000
$7,410 88,223 - - - - $7,410
88,223
kWh
-
-
MMBtu
-
-
MMBtu
02: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$12,684
Cost:
$2,350
- - - - $12,684 573 -
-
kWh
-
-
MMBtu
$12,684
573
MMBtu
03: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$11,278
Cost:
$2,350
$11,278 134,260 - - - - $11,278
134,260
kWh
-
-
MMBtu
-
-
MMBtu
04: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$2,080
Cost:
$500
$2,080 24,774 - - - - $2,080
24,774
kWh
-
-
MMBtu
-
-
MMBtu
05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$5,930
Cost:
$2,000
$5,930 70,577 - - - - $5,930
70,577
kWh
-
-
MMBtu
-
-
MMBtu
06: 2.1332 CONVERT COMBUSTION EQUIPMENT TO BURN NATURAL GAS Savings:
$27,486
Cost:
$11,000
- - $(-17,948) (-2,564) $45,434 2,564 -
-
kWh
$(-17,948)
(-2,564)
MMBtu
$45,434
2,564
MMBtu
07: 2.7444 CLOSE HOLES AND OPENINGS IN BUILDING SUCH AS BROKEN WINDOWS Savings:
$10,394
Cost:
$7,600
$10,394 123,739 - - - - $10,394
123,739
kWh
-
-
MMBtu
-
-
MMBtu
08: 2.7134 USE PHOTOCELL CONTROLS Savings:
$100
Cost:
$85
$100 1,190 - - - - $100
1,190
kWh
-
-
MMBtu
-
-
MMBtu
09: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT Savings:
$41,139
Cost:
$70,800
$63,840 760,000 $(-22,701) (-3,243) - - $63,840
760,000
kWh
$(-22,701)
(-3,243)
MMBtu
-
-
MMBtu
TOTAL RECOMMENDED Savings:
$118,501
Cost:
$98,685
$101,032 1,202,763 $(-40,649) (-5,807) $58,118 3,137 $101,032
1,202,763
kWh
$(-40,649)
(-5,807)
MMBtu
$58,118
3,137
MMBtu
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - -
-
kWh
-
-
MMBtu
-
-
MMBtu
Savings
Cost
$ kWh $ MMBtu $ MMBtu
Electricity Usage Natural Gas LPG Electricity Usage Natural Gas LPG