Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
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Assessment Year | 1989 |
Principal Product | POULTRY |
NAICS | n/a |
SIC | 2015 - Poultry Slaughtering And Processing |
Sales | $50,000,000-$100,000,000 |
# of Employees | 575 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 68,000,000 Pieces |
Production Hrs. Annual | 4,160 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $638,137 | 12,383,939 | kWh | $0.05 |
Natural Gas | $150,811 | 50,391 | MMBtu | $2.99 |
TOTAL ENERGY COSTS | $788,948 | |||
RECOMMENDED SAVINGS* | $100,230 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $85,750 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $1,040 Cost: - |
- | - | $1,940 | 650 | $(-900) | - |
- - kWh |
$1,940 650 MMBtu |
$(-900) - $ |
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02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $604 Cost: $2,400 |
$604 | 11,723 | - | - | - | - |
$604 11,723 kWh |
- - MMBtu |
- - $ |
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03: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $534 Cost: $1,020 |
- | - | $534 | 179 | - | - |
- - kWh |
$534 179 MMBtu |
- - $ |
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04: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $423 Cost: $210 |
- | - | $423 | 142 | - | - |
- - kWh |
$423 142 MMBtu |
- - $ |
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05: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS |
Savings: $219 Cost: $350 |
$219 | 4,396 | - | - | - | - |
$219 4,396 kWh |
- - MMBtu |
- - $ |
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06: 2.2624 USE COLD WASTE WATER TO COOL CHILLER FEED WATER |
Savings: $14,480 Cost: $16,950 |
$14,480 | 281,360 | - | - | - | - |
$14,480 281,360 kWh |
- - MMBtu |
- - $ |
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07: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT |
Savings: $68,230 Cost: $29,500 |
- | - | $68,230 | 22,820 | - | - |
- - kWh |
$68,230 22,820 MMBtu |
- - $ |
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08: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $14,700 Cost: - |
$14,700 | 285,463 | - | - | - | - |
$14,700 285,463 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $100,230 Cost: $50,430 |
$30,003 | 582,942 | $71,127 | 23,791 | $(-900) | - | $30,003 582,942 kWh |
$71,127 23,791 MMBtu |
$(-900) - $ |
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TOTAL IMPLEMENTED |
Savings: $85,750 Cost: $33,480 |
$15,523 | 301,582 | $71,127 | 23,791 | $(-900) | - | $15,523 301,582 kWh |
$71,127 23,791 MMBtu |
$(-900) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |