Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
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Assessment Year | 1991 |
Principal Product | PROCESSED CHICKENS |
NAICS | n/a |
SIC | 2015 - Poultry Slaughtering And Processing |
Sales | $100,000,000-$500,000,000 |
# of Employees | 950 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 234,000,000 Pieces |
Production Hrs. Annual | 6,120 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $1,564,805 | 28,439,332 | kWh | $0.06 |
Natural Gas | $154,531 | 68,129 | MMBtu | $2.27 |
Fuel Oil #2 | $2,440 | 352 | MMBtu | $6.93 |
TOTAL ENERGY COSTS | $1,721,776 | |||
RECOMMENDED SAVINGS* | $77,045 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $77,045 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $9,880 Cost: $500 |
- | - | $9,880 | 4,940 |
- - kWh |
$9,880 4,940 MMBtu |
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02: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $534 Cost: $1,330 |
- | - | $534 | 267 |
- - kWh |
$534 267 MMBtu |
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03: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $754 Cost: $150 |
- | - | $754 | 377 |
- - kWh |
$754 377 MMBtu |
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04: 2.4133 USE MOST EFFICIENT TYPE OF ELECTRIC MOTORS |
Savings: $5,147 Cost: $5,838 |
$5,147 | 93,494 | - | - |
$5,147 93,494 kWh |
- - MMBtu |
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05: 2.2447 HEAT WATER WITH EXHAUST HEAT |
Savings: $60,730 Cost: $125,000 |
- | - | $60,730 | 22,568 |
- - kWh |
$60,730 22,568 MMBtu |
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TOTAL RECOMMENDED |
Savings: $77,045 Cost: $132,818 |
$5,147 | 93,494 | $71,898 | 28,152 | $5,147 93,494 kWh |
$71,898 28,152 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $77,045 Cost: $132,818 |
$5,147 | 93,494 | $71,898 | 28,152 | $5,147 93,494 kWh |
$71,898 28,152 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |