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IAC Assessment: GT0520
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IAC Assessment: GT0520
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IAC Center Georgia Institute of Technology
Assessment Year 1994
Principal Product Filter Paper
NAICS n/a
SIC 2621 - Paper Mills
Sales $10,000,000-$50,000,000
# of Employees 62
Plant Area (Sq.Ft.) 106,000
Annual Production 9,600,000 Pounds
Production Hrs. Annual 7,560
Location (State) GA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $531,355 9,280,188 kWh $0.06
Natural Gas $354,206 101,372 MMBtu $3.49
TOTAL ENERGY COSTS $885,561
RECOMMENDED SAVINGS* $122,955 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $38,855
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$4,300
Cost:
$9,420
$4,300 75,322 - - - - $4,300
75,322
kWh
-
-
MMBtu
-
-
$
02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$460
Cost:
$835
$460 8,206 - - - - $460
8,206
kWh
-
-
MMBtu
-
-
$
03: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$9,900
Cost:
$450
- - $9,900 2,836 - - -
-
kWh
$9,900
2,836
MMBtu
-
-
$
04: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS Savings:
$3,845
Cost:
$500
- - $3,845 1,102 - - -
-
kWh
$3,845
1,102
MMBtu
-
-
$
05: 2.2163 USE MINIMUM STEAM OPERATING PRESSURE Savings:
$2,350
Cost:
-
- - $2,350 674 - - -
-
kWh
$2,350
674
MMBtu
-
-
$
06: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE Savings:
$20,350
Cost:
-
- - - - $20,350 - -
-
kWh
-
-
MMBtu
$20,350
-
$
07: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$81,750
Cost:
$124,600
$81,750 1,431,712 - - - - $81,750
1,431,712
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$122,955
Cost:
$135,805
$86,510 1,515,240 $16,095 4,612 $20,350 - $86,510
1,515,240
kWh
$16,095
4,612
MMBtu
$20,350
-
$
TOTAL IMPLEMENTED Savings:
$38,855
Cost:
$11,205
$4,760 83,528 $13,745 3,938 $20,350 - $4,760
83,528
kWh
$13,745
3,938
MMBtu
$20,350
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes