Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Georgia Institute of Technology |
---|---|
Assessment Year | 1994 |
Principal Product | Filter Paper |
NAICS | n/a |
SIC | 2621 - Paper Mills |
Sales | $10,000,000-$50,000,000 |
# of Employees | 62 |
Plant Area (Sq.Ft.) | 106,000 |
Annual Production | 9,600,000 Pounds |
Production Hrs. Annual | 7,560 |
Location (State) | GA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $531,355 | 9,280,188 | kWh | $0.06 |
Natural Gas | $354,206 | 101,372 | MMBtu | $3.49 |
TOTAL ENERGY COSTS | $885,561 | |||
RECOMMENDED SAVINGS* | $122,955 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $38,855 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $4,300 Cost: $9,420 |
$4,300 | 75,322 | - | - | - | - |
$4,300 75,322 kWh |
- - MMBtu |
- - $ |
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02: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $460 Cost: $835 |
$460 | 8,206 | - | - | - | - |
$460 8,206 kWh |
- - MMBtu |
- - $ |
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03: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $9,900 Cost: $450 |
- | - | $9,900 | 2,836 | - | - |
- - kWh |
$9,900 2,836 MMBtu |
- - $ |
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04: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $3,845 Cost: $500 |
- | - | $3,845 | 1,102 | - | - |
- - kWh |
$3,845 1,102 MMBtu |
- - $ |
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05: 2.2163 USE MINIMUM STEAM OPERATING PRESSURE |
Savings: $2,350 Cost: - |
- | - | $2,350 | 674 | - | - |
- - kWh |
$2,350 674 MMBtu |
- - $ |
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06: 2.8114 CHANGE RATE SCHEDULES OR OTHER CHANGES IN UTILITY SERVICE |
Savings: $20,350 Cost: - |
- | - | - | - | $20,350 | - |
- - kWh |
- - MMBtu |
$20,350 - $ |
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07: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM |
Savings: $81,750 Cost: $124,600 |
$81,750 | 1,431,712 | - | - | - | - |
$81,750 1,431,712 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $122,955 Cost: $135,805 |
$86,510 | 1,515,240 | $16,095 | 4,612 | $20,350 | - | $86,510 1,515,240 kWh |
$16,095 4,612 MMBtu |
$20,350 - $ |
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TOTAL IMPLEMENTED |
Savings: $38,855 Cost: $11,205 |
$4,760 | 83,528 | $13,745 | 3,938 | $20,350 | - | $4,760 83,528 kWh |
$13,745 3,938 MMBtu |
$20,350 - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |