Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Univ. of Kansas |
---|---|
Assessment Year | 1985 |
Principal Product | PLASTIC MOLDED CONTAINER |
NAICS | n/a |
SIC | 3089 - Plastics Products, Nec |
Sales | $1,000,000-$5,000,000 |
# of Employees | 25 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 2,500,000 Pounds |
Production Hrs. Annual | 6,168 |
Location (State) | MO |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $132,623 | 1,961,899 | kWh | $0.07 |
Natural Gas | $8,831 | 2,093 | MMBtu | $4.22 |
TOTAL ENERGY COSTS | $141,454 | |||
RECOMMENDED SAVINGS* | $17,952 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $15,538 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $10,210 Cost: $1,200 |
$11,430 | 169,109 | $(-1,220) | (-289) | - | - |
$11,430 169,109 kWh |
$(-1,220) (-289) MMBtu |
- - $ |
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02: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $2,813 Cost: $750 |
$2,813 | 41,618 | - | - | - | - |
$2,813 41,618 kWh |
- - MMBtu |
- - $ |
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03: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES |
Savings: $1,466 Cost: $3,000 |
$1,466 | 21,688 | - | - | - | - |
$1,466 21,688 kWh |
- - MMBtu |
- - $ |
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04: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $1,446 Cost: $600 |
$1,446 | 21,395 | - | - | - | - |
$1,446 21,395 kWh |
- - MMBtu |
- - $ |
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05: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $891 Cost: $150 |
$891 | 13,189 | - | - | - | - |
$891 13,189 kWh |
- - MMBtu |
- - $ |
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06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $260 Cost: - |
- | - | $430 | 102 | $(-170) | - |
- - kWh |
$430 102 MMBtu |
$(-170) - $ |
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07: 2.1123 INSTALL AUTOMATIC STACK DAMPER |
Savings: $688 Cost: $700 |
- | - | $688 | 163 | - | - |
- - kWh |
$688 163 MMBtu |
- - $ |
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08: 3.4154 ELIMINATE LEAKS IN WATER LINES AND VALVES |
Savings: $178 Cost: $100 |
$178 | 2,638 | - | - | - | - |
$178 2,638 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $17,952 Cost: $6,500 |
$18,224 | 269,637 | $(-102) | (-24) | $(-170) | - | $18,224 269,637 kWh |
$(-102) (-24) MMBtu |
$(-170) - $ |
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TOTAL IMPLEMENTED |
Savings: $15,538 Cost: $2,800 |
$16,758 | 247,949 | $(-1,220) | (-289) | - | - | $16,758 247,949 kWh |
$(-1,220) (-289) MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |