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IAC Assessment: KU0198
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IAC Assessment: KU0198
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IAC Center Univ. of Kansas
Assessment Year 1986
Principal Product LIQUID DETERGENT
NAICS n/a
SIC 2899 - Chemical Preparations, Nec
Sales $10,000,000-$50,000,000
# of Employees 17
Plant Area (Sq.Ft.) 0
Annual Production 38,000,000 Pounds
Production Hrs. Annual 6,000
Location (State) KS
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $24,283 582,063 kWh $0.04
Natural Gas $356,456 105,904 MMBtu $3.37
Other Energy $292,479 70,505 MMBtu $4.15
TOTAL ENERGY COSTS $673,218
RECOMMENDED SAVINGS* $56,206 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $30,094
#|Description Savings
Cost
Status Electricity Usage Natural Gas Other Energy Administrative Changes Electricity Usage Natural Gas Other Energy Administrative Changes
$ kWh $ MMBtu $ MMBtu $ $
01: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED Savings:
$26,112
Cost:
$21,000
- - - - $25,525 3,595 $587 - -
-
kWh
-
-
MMBtu
$25,525
3,595
MMBtu
$587
-
$
02: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS Savings:
$17,771
Cost:
$880
- - - - $17,771 2,503 - - -
-
kWh
-
-
MMBtu
$17,771
2,503
MMBtu
-
-
$
03: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$3,569
Cost:
-
- - $3,569 1,059 - - - - -
-
kWh
$3,569
1,059
MMBtu
-
-
MMBtu
-
-
$
04: 2.2163 USE MINIMUM STEAM OPERATING PRESSURE Savings:
$2,706
Cost:
$5,000
- - $2,706 803 - - - - -
-
kWh
$2,706
803
MMBtu
-
-
MMBtu
-
-
$
05: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$2,456
Cost:
$1,724
$2,456 58,910 - - - - - - $2,456
58,910
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
06: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$1,845
Cost:
$3,666
$1,845 44,256 - - - - - - $1,845
44,256
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
07: 2.6232 INSTALL SET-BACK TIMERS Savings:
$1,185
Cost:
$60
$1,185 28,429 - - - - - - $1,185
28,429
kWh
-
-
MMBtu
-
-
MMBtu
-
-
$
08: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS Savings:
$562
Cost:
$124
$232 5,569 $330 98 - - - - $232
5,569
kWh
$330
98
MMBtu
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$56,206
Cost:
$32,454
$5,718 137,164 $6,605 1,960 $43,296 6,098 $587 - $5,718
137,164
kWh
$6,605
1,960
MMBtu
$43,296
6,098
MMBtu
$587
-
$
TOTAL IMPLEMENTED Savings:
$30,094
Cost:
$11,454
$5,718 137,164 $6,605 1,960 $17,771 2,503 - - $5,718
137,164
kWh
$6,605
1,960
MMBtu
$17,771
2,503
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ MMBtu $ $
Electricity Usage Natural Gas Other Energy Administrative Changes Electricity Usage Natural Gas Other Energy Administrative Changes