Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Univ. of Kansas |
---|---|
Assessment Year | 1986 |
Principal Product | CORRUGATED BOXES |
NAICS | n/a |
SIC | 2653 - Corrugated And Solid Fiber Boxes |
Sales | $5,000,000-$10,000,000 |
# of Employees | 75 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 0 Units |
Production Hrs. Annual | 4,000 |
Location (State) | MO |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $34,893 | 386,870 | kWh | $0.09 |
Natural Gas | $14,966 | 3,048 | MMBtu | $4.91 |
TOTAL ENERGY COSTS | $49,859 | |||
RECOMMENDED SAVINGS* | $14,218 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $11,575 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $4,437 Cost: $2,317 |
$4,437 | 49,238 | - | - | - | - |
$4,437 49,238 kWh |
- - MMBtu |
- - $ |
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02: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS |
Savings: $3,717 Cost: $1,000 |
- | - | $3,717 | 757 | - | - |
- - kWh |
$3,717 757 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $2,773 Cost: $150 |
$2,773 | 30,774 | - | - | - | - |
$2,773 30,774 kWh |
- - MMBtu |
- - $ |
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04: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $1,162 Cost: $615 |
$1,162 | 12,896 | - | - | - | - |
$1,162 12,896 kWh |
- - MMBtu |
- - $ |
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05: 2.1123 INSTALL AUTOMATIC STACK DAMPER |
Savings: $1,085 Cost: $1,500 |
- | - | $1,085 | 221 | - | - |
- - kWh |
$1,085 221 MMBtu |
- - $ |
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06: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $648 Cost: - |
- | - | $948 | 193 | $(-300) | - |
- - kWh |
$948 193 MMBtu |
$(-300) - $ |
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07: 2.4322 USE OR REPLACE WITH ENERGY EFFICIENT SUBSTITUTES |
Savings: $396 Cost: - |
$396 | 4,396 | - | - | - | - |
$396 4,396 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $14,218 Cost: $5,582 |
$8,768 | 97,304 | $5,750 | 1,171 | $(-300) | - | $8,768 97,304 kWh |
$5,750 1,171 MMBtu |
$(-300) - $ |
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TOTAL IMPLEMENTED |
Savings: $11,575 Cost: $3,467 |
$7,210 | 80,012 | $4,665 | 950 | $(-300) | - | $7,210 80,012 kWh |
$4,665 950 MMBtu |
$(-300) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |