Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Univ. of Kansas |
---|---|
Assessment Year | 1987 |
Principal Product | CHILDREN'S GARMENTS |
NAICS | n/a |
SIC | 2361 - Girls', Children's, and Infants' Dresses, Blouses, and Shirts |
Sales | $500,000-$1,000,000 |
# of Employees | 100 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 15,000 Pieces |
Production Hrs. Annual | 2,125 |
Location (State) | NE |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $11,532 | 223,329 | kWh | $0.05 |
Natural Gas | $11,798 | 2,380 | MMBtu | $4.96 |
TOTAL ENERGY COSTS | $23,330 | |||
RECOMMENDED SAVINGS* | $3,064 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $1,409 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7221 LOWER TEMPERATURE DURING THE WINTER SEASON AND VICE-VERSA |
Savings: $1,053 Cost: - |
$121 | 2,345 | $932 | 188 | - | - |
$121 2,345 kWh |
$932 188 MMBtu |
- - $ |
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02: 2.1123 INSTALL AUTOMATIC STACK DAMPER |
Savings: $602 Cost: $1,050 |
- | - | $602 | 121 | - | - |
- - kWh |
$602 121 MMBtu |
- - $ |
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03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $590 Cost: $2,593 |
$590 | 11,430 | - | - | - | - |
$590 11,430 kWh |
- - MMBtu |
- - $ |
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04: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $351 Cost: $100 |
- | - | $451 | 91 | $(-100) | - |
- - kWh |
$451 91 MMBtu |
$(-100) - $ |
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05: 2.1123 INSTALL AUTOMATIC STACK DAMPER |
Savings: $228 Cost: $750 |
- | - | $228 | 46 | - | - |
- - kWh |
$228 46 MMBtu |
- - $ |
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06: 2.2114 SHUT OFF STEAM TRAPS ON SUPER HEATED STEAM LINES WHEN NOT IN USE |
Savings: $131 Cost: $100 |
- | - | $131 | 26 | - | - |
- - kWh |
$131 26 MMBtu |
- - $ |
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07: 2.7441 REPLACE BROKEN WINDOWS AND/OR WINDOW SASH |
Savings: $109 Cost: $250 |
- | - | $109 | 22 | - | - |
- - kWh |
$109 22 MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $3,064 Cost: $4,843 |
$711 | 13,775 | $2,453 | 494 | $(-100) | - | $711 13,775 kWh |
$2,453 494 MMBtu |
$(-100) - $ |
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TOTAL IMPLEMENTED |
Savings: $1,409 Cost: $3,793 |
$590 | 11,430 | $919 | 185 | $(-100) | - | $590 11,430 kWh |
$919 185 MMBtu |
$(-100) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |