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IAC Assessment: KU0231
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IAC Assessment: KU0231
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IAC Center Univ. of Kansas
Assessment Year 1987
Principal Product GASKET DIE CUTS
NAICS n/a
SIC 3053 - Gaskets, Packing And Sealing Devices
Sales $5,000,000-$10,000,000
# of Employees 75
Plant Area (Sq.Ft.) 0
Annual Production 65,000,000 Pieces
Production Hrs. Annual 2,125
Location (State) MO
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $31,629 350,234 kWh $0.09
Natural Gas $6,679 1,438 MMBtu $4.64
TOTAL ENERGY COSTS $38,308
RECOMMENDED SAVINGS* $7,554 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $2,424
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$4,553
Cost:
$2,059
$4,553 50,410 - - - - $4,553
50,410
kWh
-
-
MMBtu
-
-
$
02: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$847
Cost:
$100
$847 9,379 - - - - $847
9,379
kWh
-
-
MMBtu
-
-
$
03: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS Savings:
$809
Cost:
$40
$159 1,758 $650 140 - - $159
1,758
kWh
$650
140
MMBtu
-
-
$
04: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT Savings:
$445
Cost:
$600
$556 6,155 $(-111) (-24) - - $556
6,155
kWh
$(-111)
(-24)
MMBtu
-
-
$
05: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$424
Cost:
$600
$424 4,689 - - - - $424
4,689
kWh
-
-
MMBtu
-
-
$
06: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$212
Cost:
$120
$212 2,345 - - - - $212
2,345
kWh
-
-
MMBtu
-
-
$
07: 2.6121 REDUCE HOT WATER TEMPERATURE TO THE MINIMUM REQUIRED Savings:
$211
Cost:
-
$164 1,758 $47 10 - - $164
1,758
kWh
$47
10
MMBtu
-
-
$
08: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS Savings:
$132
Cost:
$250
$132 1,465 - - - - $132
1,465
kWh
-
-
MMBtu
-
-
$
09: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$(-79)
Cost:
-
- - $121 26 $(-200) - -
-
kWh
$121
26
MMBtu
$(-200)
-
$
TOTAL RECOMMENDED Savings:
$7,554
Cost:
$3,769
$7,047 77,959 $707 152 $(-200) - $7,047
77,959
kWh
$707
152
MMBtu
$(-200)
-
$
TOTAL IMPLEMENTED Savings:
$2,424
Cost:
$860
$1,806 19,929 $818 176 $(-200) - $1,806
19,929
kWh
$818
176
MMBtu
$(-200)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes