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IAC Assessment: KU0234
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IAC Assessment: KU0234
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IAC Center Univ. of Kansas
Assessment Year 1987
Principal Product CORRUGATED CONTAINERS
NAICS n/a
SIC 2653 - Corrugated And Solid Fiber Boxes
Sales $10,000,000-$50,000,000
# of Employees 100
Plant Area (Sq.Ft.) 0
Annual Production 35,000 Tons
Production Hrs. Annual 6,048
Location (State) MO
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $153,878 2,559,496 kWh $0.06
Natural Gas $181,406 38,130 MMBtu $4.76
TOTAL ENERGY COSTS $335,284
RECOMMENDED SAVINGS* $31,547 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $17,989
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$3,784
Cost:
$3,862
$3,784 63,013 - - - - $3,784
63,013
kWh
-
-
MMBtu
-
-
$
02: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT Savings:
$4,993
Cost:
$8,000
- - $4,993 1,049 - - -
-
kWh
$4,993
1,049
MMBtu
-
-
$
03: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$5,345
Cost:
$4,000
- - $5,345 1,123 - - -
-
kWh
$5,345
1,123
MMBtu
-
-
$
04: 2.1222 INSTALL TURBULATORS Savings:
$4,336
Cost:
$6,311
- - $4,336 911 - - -
-
kWh
$4,336
911
MMBtu
-
-
$
05: 2.4312 IMPROVE LUBRICATION PRACTICES Savings:
$4,229
Cost:
-
$4,229 70,340 - - - - $4,229
70,340
kWh
-
-
MMBtu
-
-
$
06: 2.2511 INSULATE BARE EQUIPMENT Savings:
$3,013
Cost:
$5,000
- - $3,013 633 - - -
-
kWh
$3,013
633
MMBtu
-
-
$
07: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$2,044
Cost:
-
$2,044 33,998 - - - - $2,044
33,998
kWh
-
-
MMBtu
-
-
$
08: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS Savings:
$1,504
Cost:
$140
- - $1,504 316 - - -
-
kWh
$1,504
316
MMBtu
-
-
$
09: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$1,385
Cost:
-
- - $1,585 333 $(-200) - -
-
kWh
$1,585
333
MMBtu
$(-200)
-
$
10: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT Savings:
$544
Cost:
$400
$758 12,603 $(-214) (-45) - - $758
12,603
kWh
$(-214)
(-45)
MMBtu
-
-
$
11: 2.6218 TURN OFF EQUIPMENT WHEN NOT IN USE Savings:
$370
Cost:
-
$370 6,155 - - - - $370
6,155
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$31,547
Cost:
$27,713
$11,185 186,109 $20,562 4,320 $(-200) - $11,185
186,109
kWh
$20,562
4,320
MMBtu
$(-200)
-
$
TOTAL IMPLEMENTED Savings:
$17,989
Cost:
$13,402
$6,956 115,769 $11,233 2,360 $(-200) - $6,956
115,769
kWh
$11,233
2,360
MMBtu
$(-200)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes