Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Univ. of Kansas |
---|---|
Assessment Year | 1988 |
Principal Product | HEAVY COMMERCIAL TRUCKS |
NAICS | n/a |
SIC | 3537 - Industrial Trucks And Tractors |
Sales | $10,000,000-$50,000,000 |
# of Employees | 150 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 750 Pieces |
Production Hrs. Annual | 4,420 |
Location (State) | KS |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $163,285 | 2,110,199 | kWh | $0.08 |
Natural Gas | $45,414 | 11,517 | MMBtu | $3.94 |
TOTAL ENERGY COSTS | $208,699 | |||
RECOMMENDED SAVINGS* | $12,968 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $8,971 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Electricity Usage | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $3,185 Cost: $2,000 |
$3,185 | 41,618 | - | - |
$3,185 41,618 kWh |
- - MMBtu |
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02: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS |
Savings: $191 Cost: - |
$159 | 2,052 | $32 | 8 |
$159 2,052 kWh |
$32 8 MMBtu |
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03: 2.2532 USE ONLY AMOUNT OF AIR NECESSARY TO PREVENT EXPLOSION HAZARD |
Savings: $1,539 Cost: - |
$46 | 586 | $1,493 | 379 |
$46 586 kWh |
$1,493 379 MMBtu |
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04: 2.7441 REPLACE BROKEN WINDOWS AND/OR WINDOW SASH |
Savings: $1,773 Cost: $1,800 |
- | - | $1,773 | 450 |
- - kWh |
$1,773 450 MMBtu |
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05: 2.6214 SHUT OFF PILOTS IN STANDBY EQUIPMENT |
Savings: $347 Cost: - |
- | - | $347 | 88 |
- - kWh |
$347 88 MMBtu |
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06: 2.1123 INSTALL AUTOMATIC STACK DAMPER |
Savings: $2,033 Cost: $2,125 |
- | - | $2,033 | 516 |
- - kWh |
$2,033 516 MMBtu |
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07: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $3,741 Cost: $1,680 |
$3,741 | 48,359 | - | - |
$3,741 48,359 kWh |
- - MMBtu |
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08: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $159 Cost: - |
$159 | 2,052 | - | - |
$159 2,052 kWh |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $12,968 Cost: $7,605 |
$7,290 | 94,667 | $5,678 | 1,441 | $7,290 94,667 kWh |
$5,678 1,441 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $8,971 Cost: $3,680 |
$7,131 | 92,615 | $1,840 | 467 | $7,131 92,615 kWh |
$1,840 467 MMBtu |
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Savings Cost |
$ | kWh | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Electricity Usage | Natural Gas |