Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Univ. of Kansas |
---|---|
Assessment Year | 1988 |
Principal Product | LAUNDRY STARCH |
NAICS | n/a |
SIC | 2842 - Polishes And Sanitation Goods |
Sales | $10,000,000-$50,000,000 |
# of Employees | 65 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 2,500,000 Pieces |
Production Hrs. Annual | 2,125 |
Location (State) | MO |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $73,779 | 706,331 | kWh | $0.10 |
Natural Gas | $74,955 | 18,497 | MMBtu | $4.05 |
TOTAL ENERGY COSTS | $148,734 | |||
RECOMMENDED SAVINGS* | $16,588 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $12,530 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $7,528 Cost: $8,010 |
$7,528 | 72,098 | - | - | - | - |
$7,528 72,098 kWh |
- - MMBtu |
- - $ |
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02: 2.2444 USE HOT PROCESS FLUIDS TO PREHEAT INCOMING PROCESS FLUIDS |
Savings: $3,098 Cost: $500 |
- | - | $3,098 | 765 | - | - |
- - kWh |
$3,098 765 MMBtu |
- - $ |
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03: 2.2414 USE WASTE HEAT FROM HOT FLUE GASES TO PREHEAT |
Savings: $2,831 Cost: $4,000 |
- | - | $2,831 | 699 | - | - |
- - kWh |
$2,831 699 MMBtu |
- - $ |
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04: 2.1131 REPAIR FAULTY INSULATION IN FURNACES, BOILERS, ETC |
Savings: $563 Cost: $936 |
- | - | $563 | 139 | - | - |
- - kWh |
$563 139 MMBtu |
- - $ |
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05: 2.2449 RECOVER HEAT FROM EXHAUSTED STEAM, HOT AIR OR HOT WATER |
Savings: $664 Cost: $800 |
- | - | $178 | 44 | $486 | - |
- - kWh |
$178 44 MMBtu |
$486 - $ |
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06: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $153 Cost: - |
$153 | 1,465 | - | - | - | - |
$153 1,465 kWh |
- - MMBtu |
- - $ |
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07: 2.4312 IMPROVE LUBRICATION PRACTICES |
Savings: $153 Cost: - |
$153 | 1,465 | - | - | - | - |
$153 1,465 kWh |
- - MMBtu |
- - $ |
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08: 2.7441 REPLACE BROKEN WINDOWS AND/OR WINDOW SASH |
Savings: $1,598 Cost: $28 |
$31 | 293 | $1,567 | 387 | - | - |
$31 293 kWh |
$1,567 387 MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $16,588 Cost: $14,274 |
$7,865 | 75,321 | $8,237 | 2,034 | $486 | - | $7,865 75,321 kWh |
$8,237 2,034 MMBtu |
$486 - $ |
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TOTAL IMPLEMENTED |
Savings: $12,530 Cost: $8,538 |
$7,865 | 75,321 | $4,665 | 1,152 | - | - | $7,865 75,321 kWh |
$4,665 1,152 MMBtu |
- - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |