Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Univ. of Kansas |
---|---|
Assessment Year | 1989 |
Principal Product | DENIM JEANS |
NAICS | n/a |
SIC | 2325 - Men's and Boys' Separate Trousers and Slacks |
Sales | $50,000,000-$100,000,000 |
# of Employees | 265 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 1,900,000 Pieces |
Production Hrs. Annual | 5,400 |
Location (State) | MO |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $100,913 | 1,785,756 | kWh | $0.06 |
Natural Gas | $78,372 | 21,012 | MMBtu | $3.73 |
TOTAL ENERGY COSTS | $179,285 | |||
RECOMMENDED SAVINGS* | $14,683 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $9,514 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $421 Cost: $121 |
$421 | 7,327 | - | - | - | - |
$421 7,327 kWh |
- - MMBtu |
- - $ |
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02: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $447 Cost: $250 |
$447 | 7,913 | - | - | - | - |
$447 7,913 kWh |
- - MMBtu |
- - $ |
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03: 2.6212 TURN OFF EQUIPMENT DURING BREAKS, REDUCE OPERATING TIME |
Savings: $315 Cost: $150 |
$315 | 5,569 | - | - | - | - |
$315 5,569 kWh |
- - MMBtu |
- - $ |
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04: 2.2113 REPAIR OR REPLACE STEAM TRAPS |
Savings: $8,388 Cost: $450 |
- | - | $8,388 | 2,249 | - | - |
- - kWh |
$8,388 2,249 MMBtu |
- - $ |
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05: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT |
Savings: $3,205 Cost: $2,400 |
- | - | $3,205 | 859 | - | - |
- - kWh |
$3,205 859 MMBtu |
- - $ |
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06: 2.1123 INSTALL AUTOMATIC STACK DAMPER |
Savings: $1,466 Cost: $1,700 |
- | - | $1,466 | 393 | - | - |
- - kWh |
$1,466 393 MMBtu |
- - $ |
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07: 2.6214 SHUT OFF PILOTS IN STANDBY EQUIPMENT |
Savings: $258 Cost: - |
- | - | $418 | 112 | $(-160) | - |
- - kWh |
$418 112 MMBtu |
$(-160) - $ |
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08: 2.2511 INSULATE BARE EQUIPMENT |
Savings: $183 Cost: $280 |
$75 | 1,465 | $108 | 29 | - | - |
$75 1,465 kWh |
$108 29 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $14,683 Cost: $5,351 |
$1,258 | 22,274 | $13,585 | 3,642 | $(-160) | - | $1,258 22,274 kWh |
$13,585 3,642 MMBtu |
$(-160) - $ |
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TOTAL IMPLEMENTED |
Savings: $9,514 Cost: $821 |
$868 | 15,240 | $8,806 | 2,361 | $(-160) | - | $868 15,240 kWh |
$8,806 2,361 MMBtu |
$(-160) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |