Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Univ. of Kansas |
---|---|
Assessment Year | 1991 |
Principal Product | AIR FILTER CANISTERS |
NAICS | n/a |
SIC | 3564 - Blowers And Fans |
Sales | $10,000,000-$50,000,000 |
# of Employees | 230 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 250,000 Pieces |
Production Hrs. Annual | 3,840 |
Location (State) | MO |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $281,040 | 3,827,960 | kWh | $0.07 |
Natural Gas | $93,985 | 31,927 | MMBtu | $2.94 |
TOTAL ENERGY COSTS | $375,025 | |||
RECOMMENDED SAVINGS* | $16,004 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $16,004 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.6232 INSTALL SET-BACK TIMERS |
Savings: $4,777 Cost: $2,460 |
$4,777 | 65,064 | - | - | - | - |
$4,777 65,064 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS |
Savings: $796 Cost: $360 |
$796 | 10,844 | - | - | - | - |
$796 10,844 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $409 Cost: - |
$435 | 5,862 | - | - | $(-26) | - |
$435 5,862 kWh |
- - MMBtu |
$(-26) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
04: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT |
Savings: $3,963 Cost: $3,800 |
- | - | $3,963 | 1,348 | - | - |
- - kWh |
$3,963 1,348 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $3,658 Cost: $500 |
$3,658 | 49,824 | - | - | - | - |
$3,658 49,824 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
06: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT |
Savings: $1,322 Cost: - |
$1,592 | 21,688 | $(-270) | (-92) | - | - |
$1,592 21,688 kWh |
$(-270) (-92) MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
07: 2.1213 DIRECT WARMEST AIR TO COMBUSTION INTAKE |
Savings: $735 Cost: $2,200 |
- | - | $735 | 250 | - | - |
- - kWh |
$735 250 MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
08: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $344 Cost: - |
$344 | 4,689 | - | - | - | - |
$344 4,689 kWh |
- - MMBtu |
- - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL RECOMMENDED |
Savings: $16,004 Cost: $9,320 |
$11,602 | 157,971 | $4,428 | 1,506 | $(-26) | - | $11,602 157,971 kWh |
$4,428 1,506 MMBtu |
$(-26) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
TOTAL IMPLEMENTED |
Savings: $16,004 Cost: $9,320 |
$11,602 | 157,971 | $4,428 | 1,506 | $(-26) | - | $11,602 157,971 kWh |
$4,428 1,506 MMBtu |
$(-26) - $ |
|||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |