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IAC Assessment: KU0352
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IAC Assessment: KU0352
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IAC Center Univ. of Kansas
Assessment Year 1991
Principal Product AIR FILTER CANISTERS
NAICS n/a
SIC 3564 - Blowers And Fans
Sales $10,000,000-$50,000,000
# of Employees 230
Plant Area (Sq.Ft.) 0
Annual Production 250,000 Pieces
Production Hrs. Annual 3,840
Location (State) MO
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $281,040 3,827,960 kWh $0.07
Natural Gas $93,985 31,927 MMBtu $2.94
TOTAL ENERGY COSTS $375,025
RECOMMENDED SAVINGS* $16,004 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $16,004
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.6232 INSTALL SET-BACK TIMERS Savings:
$4,777
Cost:
$2,460
$4,777 65,064 - - - - $4,777
65,064
kWh
-
-
MMBtu
-
-
$
02: 2.7111 REDUCE ILLUMINATION TO MINIMUM NECESSARY LEVELS Savings:
$796
Cost:
$360
$796 10,844 - - - - $796
10,844
kWh
-
-
MMBtu
-
-
$
03: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$409
Cost:
-
$435 5,862 - - $(-26) - $435
5,862
kWh
-
-
MMBtu
$(-26)
-
$
04: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$3,963
Cost:
$3,800
- - $3,963 1,348 - - -
-
kWh
$3,963
1,348
MMBtu
-
-
$
05: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$3,658
Cost:
$500
$3,658 49,824 - - - - $3,658
49,824
kWh
-
-
MMBtu
-
-
$
06: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT Savings:
$1,322
Cost:
-
$1,592 21,688 $(-270) (-92) - - $1,592
21,688
kWh
$(-270)
(-92)
MMBtu
-
-
$
07: 2.1213 DIRECT WARMEST AIR TO COMBUSTION INTAKE Savings:
$735
Cost:
$2,200
- - $735 250 - - -
-
kWh
$735
250
MMBtu
-
-
$
08: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$344
Cost:
-
$344 4,689 - - - - $344
4,689
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$16,004
Cost:
$9,320
$11,602 157,971 $4,428 1,506 $(-26) - $11,602
157,971
kWh
$4,428
1,506
MMBtu
$(-26)
-
$
TOTAL IMPLEMENTED Savings:
$16,004
Cost:
$9,320
$11,602 157,971 $4,428 1,506 $(-26) - $11,602
157,971
kWh
$4,428
1,506
MMBtu
$(-26)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes