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IAC Assessment: KU0366
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IAC Assessment: KU0366
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IAC Center Univ. of Kansas
Assessment Year 1992
Principal Product CONFECTIONERY ITEMS
NAICS n/a
SIC 2064 - Candy & Other Confectionery Products
Sales $5,000,000-$10,000,000
# of Employees 65
Plant Area (Sq.Ft.) 0
Annual Production 4,500,000 Pounds
Production Hrs. Annual 2,125
Location (State) KS
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $127,809 2,807,151 kWh $0.05
Natural Gas $58,893 15,195 MMBtu $3.88
TOTAL ENERGY COSTS $186,702
RECOMMENDED SAVINGS* $8,660 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* -
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE Savings:
$3,148
Cost:
$6,400
$3,148 69,168 - - - - $3,148
69,168
kWh
-
-
MMBtu
-
-
$
02: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS Savings:
$1,539
Cost:
$760
$627 13,775 $912 235 - - $627
13,775
kWh
$912
235
MMBtu
-
-
$
03: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$830
Cost:
$150
- - $830 214 - - -
-
kWh
$830
214
MMBtu
-
-
$
04: 2.1222 INSTALL TURBULATORS Savings:
$621
Cost:
$1,320
- - $621 160 - - -
-
kWh
$621
160
MMBtu
-
-
$
05: 2.1232 KEEP BOILER TUBES CLEAN Savings:
$559
Cost:
$450
- - $559 144 - - -
-
kWh
$559
144
MMBtu
-
-
$
06: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$694
Cost:
$200
$694 15,240 - - - - $694
15,240
kWh
-
-
MMBtu
-
-
$
07: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$407
Cost:
$350
- - $407 105 - - -
-
kWh
$407
105
MMBtu
-
-
$
08: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$267
Cost:
$75
$267 5,862 - - - - $267
5,862
kWh
-
-
MMBtu
-
-
$
09: 2.4221 INSTALL COMPRESSOR AIR INTAKES IN COOLEST LOCATIONS Savings:
$267
Cost:
$170
$267 5,862 - - - - $267
5,862
kWh
-
-
MMBtu
-
-
$
10: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$(-45)
Cost:
-
$56 1,172 - - $(-101) - $56
1,172
kWh
-
-
MMBtu
$(-101)
-
$
11: 2.6232 INSTALL SET-BACK TIMERS Savings:
$240
Cost:
$600
$240 5,275 - - - - $240
5,275
kWh
-
-
MMBtu
-
-
$
12: 2.2437 RECOVER WASTE HEAT FROM EQUIPMENT Savings:
$133
Cost:
$200
$133 2,931 - - - - $133
2,931
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$8,660
Cost:
$10,675
$5,432 119,285 $3,329 858 $(-101) - $5,432
119,285
kWh
$3,329
858
MMBtu
$(-101)
-
$
TOTAL IMPLEMENTED Savings:
-
Cost:
-
- - - - - - -
-
kWh
-
-
MMBtu
-
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes