Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Univ. of Kansas |
---|---|
Assessment Year | 1993 |
Principal Product | BIB OVERALLS |
NAICS | n/a |
SIC | 2326 - Men's and Boys' Work Clothing |
Sales | $5,000,000-$10,000,000 |
# of Employees | 132 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 377,000 Pieces |
Production Hrs. Annual | 1,920 |
Location (State) | KS |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $54,856 | 503,810 | kWh | $0.11 |
Natural Gas | $4,311 | 946 | MMBtu | $4.56 |
TOTAL ENERGY COSTS | $59,167 | |||
RECOMMENDED SAVINGS* | $9,241 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $4,130 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
02: 2.7261 INSTALL TIMERS AND/OR THERMOSTATS |
Savings: $3,692 Cost: $4,410 |
$3,542 | 32,532 | $150 | 33 | - | - |
$3,542 32,532 kWh |
$150 33 MMBtu |
- - $ |
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03: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT |
Savings: $2,070 Cost: $1,281 |
$2,521 | 23,154 | $(-451) | (-99) | - | - |
$2,521 23,154 kWh |
$(-451) (-99) MMBtu |
- - $ |
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04: 2.1311 REPLACE ELECTRICALLY-OPERATED EQUIPMENT WITH FOSSIL FUEL EQUIPMENT |
Savings: $1,732 Cost: $1,316 |
$2,106 | 19,343 | $(-374) | (-82) | - | - |
$2,106 19,343 kWh |
$(-374) (-82) MMBtu |
- - $ |
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05: 2.7135 INSTALL OCCUPANCY SENSORS |
Savings: $1,181 Cost: $1,200 |
$1,181 | 10,844 | - | - | - | - |
$1,181 10,844 kWh |
- - MMBtu |
- - $ |
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06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $46 Cost: - |
$135 | 1,172 | - | - | $(-89) | - |
$135 1,172 kWh |
- - MMBtu |
$(-89) - $ |
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07: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $128 Cost: $350 |
$128 | 1,172 | - | - | - | - |
$128 1,172 kWh |
- - MMBtu |
- - $ |
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08: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $292 Cost: $70 |
- | - | $292 | 64 | - | - |
- - kWh |
$292 64 MMBtu |
- - $ |
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09: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $100 Cost: $88 |
- | - | $100 | 22 | - | - |
- - kWh |
$100 22 MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $9,241 Cost: $8,715 |
$9,613 | 88,217 | $(-283) | (-62) | $(-89) | - | $9,613 88,217 kWh |
$(-283) (-62) MMBtu |
$(-89) - $ |
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TOTAL IMPLEMENTED |
Savings: $4,130 Cost: $4,568 |
$3,677 | 33,704 | $542 | 119 | $(-89) | - | $3,677 33,704 kWh |
$542 119 MMBtu |
$(-89) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |