Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Louisiana State University |
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Assessment Year | 2019 |
Principal Product | Ground Coffee |
NAICS | 311920 - Coffee and Tea Manufacturing |
SIC | 2095 - Roasted Coffee |
Sales | $10,000,000-$50,000,000 |
# of Employees | 10 |
Plant Area (Sq.Ft.) | 20,000 |
Annual Production | 1,500,000 Pounds |
Production Hrs. Annual | 2,210 |
Location (State) | LA |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $12,615 | 117,760 | kWh | $0.11 |
Electricity Demand | $3,864 | 636 | kW-months/year | $6.08 |
Natural Gas | $15,522 | 2,062 | MMBtu | $7.53 |
LPG | $32,000 | 6,400 | MMBtu | $5.00 |
Fuel Oil #2 | $30,000 | 6,000 | MMBtu | $5.00 |
Other Energy | $6,000 | 1,200 | MMBtu | $5.00 |
TOTAL ENERGY COSTS | $100,001 | |||
RECOMMENDED SAVINGS* | $4,023 | *Non-energy impacts included in savings. See recommendations below |
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IMPLEMENTED SAVINGS* | $1,019 |
#|Description |
Savings Cost |
Status | Electricity Usage | Electricity Demand | Natural Gas | Electricity Usage | Electricity Demand | Natural Gas | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | kW-months/year | $ | MMBtu | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.6231 UTILIZE CONTROLS TO OPERATE EQUIPMENT ONLY WHEN NEEDED |
Savings: $1,079 Cost: $150 |
$1,079 | 10,083 | - | - | - | - |
$1,079 10,083 kWh |
- - kW-months/year |
- - MMBtu |
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02: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED |
Savings: $135 Cost: - |
$135 | 1,260 | - | - | - | - |
$135 1,260 kWh |
- - kW-months/year |
- - MMBtu |
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03: 3.7312 IMPLEMENT A REGULAR MAINTENANCE PROGRAM TO REDUCE EMISSIONS FROM LEAKY VALVES AND PIPE FITTINGS |
Savings: $839 Cost: - |
$839 | 7,833 | - | - | - | - |
$839 7,833 kWh |
- - kW-months/year |
- - MMBtu |
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04: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $480 Cost: $240 |
- | - | - | - | $480 | 64 |
- - kWh |
- - kW-months/year |
$480 64 MMBtu |
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05: 2.6218 TURN OFF EQUIPMENT WHEN NOT IN USE |
Savings: $45 Cost: - |
$45 | 423 | - | - | - | - |
$45 423 kWh |
- - kW-months/year |
- - MMBtu |
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06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS |
Savings: $1,445 Cost: $2,189 |
$1,080 | 10,091 | $365 | 60 | - | - |
$1,080 10,091 kWh |
$365 60 kW-months/year |
- - MMBtu |
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TOTAL RECOMMENDED |
Savings: $4,023 Cost: $2,579 |
$3,178 | 29,690 | $365 | 60 | $480 | 64 | $3,178 29,690 kWh |
$365 60 kW-months/year |
$480 64 MMBtu |
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TOTAL IMPLEMENTED |
Savings: $1,019 Cost: - |
$1,019 | 9,516 | - | - | - | - | $1,019 9,516 kWh |
- - kW-months/year |
- - MMBtu |
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Savings Cost |
$ | kWh | $ | kW-months/year | $ | MMBtu | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Electricity Demand | Natural Gas | Electricity Usage | Electricity Demand | Natural Gas |