Implementation Grant Funding Opportunity Open
IMPORTANT: The grant program operates on a rolling basis and applications may be submitted at any time, with quarterly reviews.
Learn More
Implementation Grant Funding Opportunity Open
Qualifying* small and medium-sized US manufacturers, that received IAC or Combined Heat and Power Technical Assistance Partnership assessments between 2018 and 2024, can now apply for grants for implementation of assessment recommendations up 50% of qualifying* project costs with a maximum of $300,000 per manufacturer.
IMPORTANT: The grant program now operates on a rolling basis and applications may be submitted at any time through the year, with quarterly reviews.
*See Full Grant Solicitation for full qualification and selection details.
IAC Center | Louisiana Tech |
---|---|
Assessment Year | 1986 |
Principal Product | POULTRY FEED |
NAICS | n/a |
SIC | 2048 - Prepared Feeds, Nec |
Sales | $50,000,000-$100,000,000 |
# of Employees | 235 |
Plant Area (Sq.Ft.) | 0 |
Annual Production | 350,000 Tons |
Production Hrs. Annual | 7,114 |
Location (State) | TX |
Source | Yearly Cost | Usage | Unit | Unit Cost |
---|---|---|---|---|
Electricity Usage | $540,304 | 11,791,911 | kWh | $0.05 |
Natural Gas | $221,013 | 49,369 | MMBtu | $4.48 |
TOTAL ENERGY COSTS | $761,317 | |||
RECOMMENDED SAVINGS* | $33,062 | *Non-energy impacts included in savings. See recommendations below |
||
IMPLEMENTED SAVINGS* | $10,624 |
#|Description |
Savings Cost |
Status | Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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$ | kWh | $ | MMBtu | $ | $ | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
01: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO |
Savings: $3,015 Cost: - |
- | - | $3,615 | 807 | $(-600) | - |
- - kWh |
$3,615 807 MMBtu |
$(-600) - $ |
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02: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED |
Savings: $1,452 Cost: - |
- | - | $1,452 | 324 | - | - |
- - kWh |
$1,452 324 MMBtu |
- - $ |
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03: 2.1243 USE HEAT FROM BOILER BLOWDOWN TO PREHEAT BOILER FEED WATER |
Savings: $9,811 Cost: $8,000 |
- | - | $9,811 | 2,190 | - | - |
- - kWh |
$9,811 2,190 MMBtu |
- - $ |
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04: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS |
Savings: $848 Cost: $140 |
- | - | $848 | 189 | - | - |
- - kWh |
$848 189 MMBtu |
- - $ |
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05: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES |
Savings: $1,025 Cost: $113 |
- | - | $1,025 | 229 | - | - |
- - kWh |
$1,025 229 MMBtu |
- - $ |
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06: 2.3212 OPTIMIZE PLANT POWER FACTOR |
Savings: $12,627 Cost: $7,140 |
$12,627 | - | - | - | - | - |
$12,627 - kWh |
- - MMBtu |
- - $ |
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07: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS |
Savings: $3,034 Cost: $422 |
$3,034 | 70,340 | - | - | - | - |
$3,034 70,340 kWh |
- - MMBtu |
- - $ |
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08: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES |
Savings: $1,250 Cost: - |
$1,250 | 36,635 | - | - | - | - |
$1,250 36,635 kWh |
- - MMBtu |
- - $ |
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TOTAL RECOMMENDED |
Savings: $33,062 Cost: $15,815 |
$16,911 | 106,975 | $16,751 | 3,739 | $(-600) | - | $16,911 106,975 kWh |
$16,751 3,739 MMBtu |
$(-600) - $ |
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TOTAL IMPLEMENTED |
Savings: $10,624 Cost: $675 |
$4,284 | 106,975 | $6,940 | 1,549 | $(-600) | - | $4,284 106,975 kWh |
$6,940 1,549 MMBtu |
$(-600) - $ |
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Savings Cost |
$ | kWh | $ | MMBtu | $ | $ | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Electricity Usage | Natural Gas | Administrative Changes | Electricity Usage | Natural Gas | Administrative Changes |