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IAC Assessment: LT0051
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IAC Assessment: LT0051
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IAC Center Louisiana Tech
Assessment Year 1986
Principal Product POULTRY FEED
NAICS n/a
SIC 2048 - Prepared Feeds, Nec
Sales $50,000,000-$100,000,000
# of Employees 235
Plant Area (Sq.Ft.) 0
Annual Production 350,000 Tons
Production Hrs. Annual 7,114
Location (State) TX
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $540,304 11,791,911 kWh $0.05
Natural Gas $221,013 49,369 MMBtu $4.48
TOTAL ENERGY COSTS $761,317
RECOMMENDED SAVINGS* $33,062 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $10,624
#|Description Savings
Cost
Status Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes
$ kWh $ MMBtu $ $
01: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$3,015
Cost:
-
- - $3,615 807 $(-600) - -
-
kWh
$3,615
807
MMBtu
$(-600)
-
$
02: 2.2121 INCREASE AMOUNT OF CONDENSATE RETURNED Savings:
$1,452
Cost:
-
- - $1,452 324 - - -
-
kWh
$1,452
324
MMBtu
-
-
$
03: 2.1243 USE HEAT FROM BOILER BLOWDOWN TO PREHEAT BOILER FEED WATER Savings:
$9,811
Cost:
$8,000
- - $9,811 2,190 - - -
-
kWh
$9,811
2,190
MMBtu
-
-
$
04: 2.2135 REPAIR AND ELIMINATE STEAM LEAKS Savings:
$848
Cost:
$140
- - $848 189 - - -
-
kWh
$848
189
MMBtu
-
-
$
05: 2.2136 INSTALL / REPAIR INSULATION ON STEAM LINES Savings:
$1,025
Cost:
$113
- - $1,025 229 - - -
-
kWh
$1,025
229
MMBtu
-
-
$
06: 2.3212 OPTIMIZE PLANT POWER FACTOR Savings:
$12,627
Cost:
$7,140
$12,627 - - - - - $12,627
-
kWh
-
-
MMBtu
-
-
$
07: 2.4111 UTILIZE ENERGY-EFFICIENT BELTS AND OTHER IMPROVED MECHANISMS Savings:
$3,034
Cost:
$422
$3,034 70,340 - - - - $3,034
70,340
kWh
-
-
MMBtu
-
-
$
08: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$1,250
Cost:
-
$1,250 36,635 - - - - $1,250
36,635
kWh
-
-
MMBtu
-
-
$
TOTAL RECOMMENDED Savings:
$33,062
Cost:
$15,815
$16,911 106,975 $16,751 3,739 $(-600) - $16,911
106,975
kWh
$16,751
3,739
MMBtu
$(-600)
-
$
TOTAL IMPLEMENTED Savings:
$10,624
Cost:
$675
$4,284 106,975 $6,940 1,549 $(-600) - $4,284
106,975
kWh
$6,940
1,549
MMBtu
$(-600)
-
$
Savings
Cost
$ kWh $ MMBtu $ $
Electricity Usage Natural Gas Administrative Changes Electricity Usage Natural Gas Administrative Changes