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IAC Assessment: MA0614
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IAC Assessment: MA0614
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IAC Center University of Massachusetts
Assessment Year 2007
Principal Product Milk, milk by-products, drinks
NAICS 311511 - Fluid Milk Manufacturing
SIC 2026 - Fluid Milk
Sales $100,000,000-$500,000,000
# of Employees 215
Plant Area (Sq.Ft.) 93,500
Annual Production 43,000 Thousand Gallons
Production Hrs. Annual 7,488
Location (State) MA
Source Yearly Cost Usage Unit Unit Cost
Electricity Usage $1,417,902 12,674,438 kWh $0.11
Electricity Demand $88,743 25,284 kW-months/year $3.51
Electricity Fees $112,272 - $ -
Natural Gas $16,942 1,248 MMBtu $13.58
Fuel Oil #2 $385,653 27,872 MMBtu $13.84
TOTAL ENERGY COSTS $2,021,512
RECOMMENDED SAVINGS* $66,543 *Non-energy impacts
included in savings.
See recommendations below
IMPLEMENTED SAVINGS* $55,751
#|Description Savings
Cost
Status Electricity Usage Electricity Demand Fuel Oil #2 Electricity Usage Electricity Demand Fuel Oil #2
$ kWh $ kW-months/year $ MMBtu
01: 2.2621 MODIFY REFRIGERATION SYSTEM TO OPERATE AT A LOWER PRESSURE Savings:
$16,978
Cost:
$5,000
$16,978 171,500 - - - - $16,978
171,500
kWh
-
-
kW-months/year
-
-
MMBtu
02: 2.1233 ANALYZE FLUE GAS FOR PROPER AIR/FUEL RATIO Savings:
$13,036
Cost:
$8,400
- - - - $13,036 1,053 -
-
kWh
-
-
kW-months/year
$13,036
1,053
MMBtu
03: 2.2622 REPLACE EXISTING CHILLER WITH HIGH EFFICIENCY MODEL Savings:
$12,870
Cost:
-
$12,870 130,000 - - - - $12,870
130,000
kWh
-
-
kW-months/year
-
-
MMBtu
04: 2.4236 ELIMINATE LEAKS IN INERT GAS AND COMPRESSED AIR LINES/ VALVES Savings:
$7,118
Cost:
$1,600
$7,118 71,900 - - - - $7,118
71,900
kWh
-
-
kW-months/year
-
-
MMBtu
05: 2.4231 REDUCE THE PRESSURE OF COMPRESSED AIR TO THE MINIMUM REQUIRED Savings:
$6,416
Cost:
$9,000
$6,078 61,400 $338 98 - - $6,078
61,400
kWh
$338
98
kW-months/year
-
-
MMBtu
06: 2.7142 UTILIZE HIGHER EFFICIENCY LAMPS AND/OR BALLASTS Savings:
$5,749
Cost:
$31,477
$5,445 55,000 $304 88 - - $5,445
55,000
kWh
$304
88
kW-months/year
-
-
MMBtu
07: 2.4146 USE ADJUSTABLE FREQUENCY DRIVE OR MULTIPLE SPEED MOTORS ON EXISTING SYSTEM Savings:
$4,376
Cost:
$20,000
$4,376 44,200 - - - - $4,376
44,200
kWh
-
-
kW-months/year
-
-
MMBtu
TOTAL RECOMMENDED Savings:
$66,543
Cost:
$75,477
$52,865 534,000 $642 186 $13,036 1,053 $52,865
534,000
kWh
$642
186
kW-months/year
$13,036
1,053
MMBtu
TOTAL IMPLEMENTED Savings:
$55,751
Cost:
$46,477
$42,411 428,400 $304 88 $13,036 1,053 $42,411
428,400
kWh
$304
88
kW-months/year
$13,036
1,053
MMBtu
Savings
Cost
$ kWh $ kW-months/year $ MMBtu
Electricity Usage Electricity Demand Fuel Oil #2 Electricity Usage Electricity Demand Fuel Oil #2